ASN Wikibase Occurrence # 132007
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Date: | Tuesday 23 February 1993 |
Time: | 14:30 LT |
Type: | Rand Robinson KR-1 |
Owner/operator: | Robert O. Woodward |
Registration: | N9HD |
MSN: | 001 |
Total airframe hrs: | 56 hours |
Engine model: | Revmaster 2100 CC |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Prescott, AZ -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | (KPRC) |
Destination airport: | (KPRC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE EXPERIMENTAL HOMEBUILT HAD ONLY BEEN OPERATED ABOUT 56 HOURS IN THE LAST 12 YEARS, WITH THE LAST FLIGHT PRIOR TO THE ACCIDENT LISTED IN THE AIRCRAFT LOG BOOK AS JUNE 16, 1992. THE PILOT MADE NO STATEMENT REGARDING THE ACCIDENT CIRCUMSTANCES. GROUND WITNESSES REPORTED HEARING AND OBSERVING THE AIRCRAFT DESCEND INTO A RESIDENTIAL AREA WITHOUT ANY APPARENT ENGINE POWER. FAA AIRWORTHINESS INSPECTORS EXAMINED THE AIRCRAFT AND REPORTED FINDING MANY DISCREPANCIES IN THE AIRCRAFT SYSTEM DESIGNS AND INSTALLATIONS. THE FUEL SYSTEM CONSISTED OF A RUBBERMAID FIVE GALLON CONTAINER CONNECTED TO THE ENGINE WITH PLASTIC TUBING AND OPERATED BY A HAND WOBBLE PUMP. THE CARBURETOR HEAT SYSTEM CONSISTED OF PVC PLUMBING PIPE HELD TOGETHER AND SECURED TO BOTH THE ENGINE EXHAUST SYSTEM AND THE CARBURETOR WITH RTV SEALANT. THE FAA INSPECTORS REPORTED THAT THE EXAMINATION OF THE REVMASTER VW ENGINE ITSELF REVEALED NO EVIDENCE OF A MECHANICAL MALFUNCTION. REVIEW OF FAA RECORDS REVEALED THAT THE PILOT'S MEDICAL HAD EXPIRED. THE PILOT HAD HELD HIS PRIVATE CERTIFICATE FOR 40 YEARS AND HAD FLOWN 290 HOURS IN THAT TIME. THE AVAILABLE PILOT AND AIRCRAFT RECORDS DISCLOSED THAT THE PILOT HAD NOT FLOWN IN THE LAST SEVEN MONTHS.
Probable Cause: THE TOTAL LOSS OF ENGINE POWER FOR UNDETERMINED REASONS. A FACTOR IN THE ACCIDENT WAS THE LACK OF A SUITABLE LANDING AREA AT THE TIME OF THE POWER INTERRUPTION.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX93LA135 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB LAX93LA135
Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Apr-2024 15:34 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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