ASN Wikibase Occurrence # 132879
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Date: | Monday 12 September 1994 |
Time: | 08:45 LT |
Type: | Beechcraft C35 Bonanza |
Owner/operator: | Daniel N. Sinclair |
Registration: | N622D |
MSN: | D2882 |
Total airframe hrs: | 4700 hours |
Engine model: | CONTINENTAL E-185 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Borrego Springs, CA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Carlsbad, CA (KCRQ) |
Destination airport: | Blythe, CA (KBLH) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:IN CRUISE OVER THE MOUNTAINS, THE FUEL PRESSURE DECREASED AND THE ENGINE QUIT. ATTEMPTS TO RESTORE POWER BY ACTIVATING THE HAND OPERATED PUMP ON THE FUEL SELECTOR AND SWITCHING BETWEEN TANKS WERE FUTILE. THE PILOT SPOTTED THE DESERT FLOOR AIRPORT JUST BEYOND THE MOUNTAINS AND ATTEMPTED A FORCED LANDING ON RUNWAY 25; HOWEVER, HE LANDED 100 YARDS SHORT IN ROUGH DESERT TERRAIN. FAA INSPECTORS FOUND THE FUEL SELECTOR VALVE ON THE RIGHT TANK AND THE SELECTOR HANDLE EXTENDED INTO THE PUMP OPERATING POSITION. NO FUEL WAS FOUND IN THE RIGHT TANK, WITH NO EVIDENCE OF SPILLAGE NOTED ON THE SURROUNDING GROUND. THE LEFT FUEL TANK CONTAINED ABOUT 1/4 TO 1/2 CAPACITY. THE ENGINE-DRIVEN FUEL PUMP AND THE COMBINED FUEL SELECTOR VALVE AND HAND FUEL PUMP WERE FOUND TO FUNCTION. THE COMBINATION FUEL SELECTOR AND HAND OPERATED FUEL PUMP UNIT HAS TWO SEPARATE MODES. WITH THE HANDLE IN THE DOWN POSITION, THE UNIT IS A FUEL SELECTOR VALVE. WHEN THE HANDLE IS EXTENDED INTO THE PUMP POSITION, THE FUEL SELECTOR VALVE MODE IS DISABLED. THE PILOT PURCHASED THE AIRCRAFT ABOUT 3 WEEKS PRIOR TO THE ACCIDENT AND HAS ONLY 6 HOURS IN THE AIRCRAFT.
Probable Cause: The pilot's inadvertent allowance of a fuel starvation loss of power event and his failure to select a tank containing fuel due to his lack of knowledge about the fuel pump/selector unit operating limitations. Factors in the accident were his limited experience in the aircraft.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX94LA363 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB LAX94LA363
Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Apr-2024 19:17 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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