Accident Rihn DR-107 One Design N857JA,
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ASN Wikibase Occurrence # 133288
 
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Date:Sunday 17 January 1999
Time:14:30 LT
Type:Silhouette image of generic RODS model; specific model in this crash may look slightly different    
Rihn DR-107 One Design
Owner/operator:James G Abraham Ii
Registration: N857JA
MSN: 0004
Total airframe hrs:66 hours
Engine model:Lycoming IO-360
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:No Las Vegas, NV -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:(KVGT)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot indicated the purpose of the flight was to practice outside snap rolls. When he pressed on the left rudder pedal, it went all the way to the floor with no resistance. He reported that the airplane was in straight and level flight when he reached down to verify that the cable was detached, hoping to be able to control the airplane when he realized that the cable was slack from the rear of the airplane. He then informed the tower of the emergency. The airplane entered a right bank from which the pilot could not recover and he jumped out of the airplane and parachuted to safety. The airplane wreckage was examined. The right rudder cable was found continuous from the cockpit pedal to the rudder control horn, with the horn end of the cable secured with a nicopress fitting. The left rudder cable was attached to the cockpit pedal but was detached from the rudder horn. The left cable to horn nicopress fitting was not on the cable's horn end and the left rudder cable end exhibited long and even splaying. When the cable was stretched out, it went all the way back to the rudder horn and was nearly identical in length to the right cable. A search of the accident site failed to locate the missing nicopress fitting.

Probable Cause: The separation of the left rudder control cable from the rudder horn due to the improper installation of a nicopress fitting that secured the cable to the control horn.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX99LA074
Status: Investigation completed
Duration: 1 year and 10 months
Download report: Final report

Sources:

NTSB LAX99LA074

Location

Revision history:

Date/timeContributorUpdates
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
25-Nov-2017 12:49 ASN Update Bot Updated [Cn, Operator, Departure airport, Destination airport, Source, Narrative, Plane category]
14-Dec-2017 16:57 ASN Update Bot Updated [Cn, Operator, Departure airport, Destination airport, Narrative]
08-Apr-2024 10:37 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Departure airport, Source, Narrative, Category, Accident report]

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