ASN Wikibase Occurrence # 133334
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 30 April 1999 |
Time: | 13:13 LT |
Type: | Cessna T210L |
Owner/operator: | Kirtland Afb Aero Club |
Registration: | N59235 |
MSN: | 2106171 |
Total airframe hrs: | 5405 hours |
Engine model: | Continental TSIO-520-H |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Albuquerque, NM -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | (KABQ) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot said that the takeoff was uneventful, and he began to level off at 1,000 feet agl to stay in the traffic pattern. He reduced the manifold pressure and began to lean the fuel mixture for cruise with the aid of the engine analyzer. After several communications with the tower, he turned the vernier mixture control further in the lean direction. The pilot said that the engine completely lost power without warning. The passenger stated that the engine fuel flow gauge 'was not indicating any fuel flow,' and the fuel mixture control was in the idle cut-off position. The pilot turned on the auxiliary fuel pump for an engine restart, but didn't move the mixture. The pilot performed a forced landing to 2 to 4 foot sand dune covered terrain. The manufacturer expanded the emergency procedure checklist, in later model T210's, to include 'mixture lean from full rich until restart occurs.' The pilot had 15 hours of flight experience in the airplane, and he had not flown it in the previous 90 days. The engine was placed on a engine run test stand, and it performed normally through its full operating range without difficulty.
Probable Cause: The pilot's improper mixture control use and the engine's subsequent power loss due to fuel starvation, and the lack of suitable terrain for the pilot to perform a forced landing. Factors were the pilot's lack of recent experience in type of airplane, the inadequate manufacturer's emergency engine airborne restart information in the Owner's Manual, and the pilot not performing the published emergency procedures for airborne engine restart.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN99LA070 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB DEN99LA070
Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Jun-2017 06:32 |
beaverspotter |
Updated [Cn, Narrative] |
26-Nov-2017 12:42 |
ASN Update Bot |
Updated [Cn, Source, Narrative] |
08-Apr-2024 06:24 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation