ASN Wikibase Occurrence # 133663
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 10 September 1998 |
Time: | 16:00 LT |
Type: | Glasair II |
Owner/operator: | Allen J. Wood |
Registration: | N51AJ |
MSN: | 391 |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Holly Hill, SC -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot had landed, and elected to abort and go around. According to witnesses, the airplane had landed long and could not make a complete stop on the available runway. The aircraft bounced three times and on the third bounce the pilot lowered the tail wheel, and the main landing gear came off the ground., The pilot attempted a go around and powered up with 300 feet of runway remaining. He attempted to clear trees at the end of the runway by pulling the nose up abruptly, then pushing the nose over after clearing the trees. At this point the engine quit momentarily. The airplane impacted the ground on fairway No. 3 at a golf course, and came to rest at the base of a pine tree. Examination of the wreckage revealed that no obvious discrepancies were found in the fuel system or the engine. Fuel was found, and examination of the carburetor and fuel pump did not show any discrepancies. The FAA inspector stated, '...the pilot was released from the hospital on September 20, 1998. All attempts to talk to [him] have failed...it appears after checking with Airman and Aircraft records [the pilot] was operating his aircraft with a non-current registration and with a denied medical.' The pilot did not return the NTSB Form 6120.1/2, and his account of the accident are not known.
Probable Cause: The pilot's failure to maintain airspeed, and his failure to perform a go-around. The pilot's misjudgment of speed and distance during the landing is a contributing factor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA98LA245 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB MIA98LA245
Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
06-Apr-2024 10:12 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation