ASN Wikibase Occurrence # 133746
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Date: | Friday 17 April 1998 |
Time: | 16:45 LT |
Type: | Monnett Sonerai II-L |
Owner/operator: | Robert G. Jaeger |
Registration: | N247RJ |
MSN: | 999 |
Total airframe hrs: | 161 hours |
Engine model: | VOLKSWAGEN 2020 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Bicknell, IN -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Junction City, KY (DVK |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While at cruise altitude, the pilot said he noticed a burning smell after he had operated the experimental airplane's auxiliary fuel pump. He said he did not notice any changes in the engine indications. He said, 'Approximately 1-minute later I noticed the reduction in engine power... .' He said he decided to make a precautionary landing on a road. When the pilot reduced the engine's power setting, the engine experienced a total loss of power. The pilot said the airplane '...built up excessive speed...' during its descent. During the landing, the airplane encountered ground affect and did not touch down as the pilot had intended. While in ground affect the airplane collided with a telephone pole and bridge frame before colliding with a ditch and coming to rest. The on-scene investigation revealed that the airplane's engine driven magneto experienced a drive coupling failure. The coupling had fractured into 4 pieces. One face on two of the four pieces had a surface with beach marks on them and no shear lips along their edges. These two faces matched each other. The remaining fracture surfaces had a coarse texture with shear lips along their edges.
Probable Cause: The pilot misjudged his altitude and airspeed during an emergency landing attempt. Factors associated with this accident were a manufacturing defect in the magneto drive coupling and a total failure of the ignition system.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI98LA128 |
Status: | Investigation completed |
Duration: | 2 years and 10 months |
Download report: | Final report |
|
Sources:
NTSB CHI98LA128
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Apr-2024 13:42 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Source, Narrative, Category, Accident report] |
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