Accident Piper PA-32R-301 N192SP,
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ASN Wikibase Occurrence # 134644
 
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Date:Friday 21 September 2001
Time:17:56
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R-301
Owner/operator:Private
Registration: N192SP
MSN: 32R-13039
Year of manufacture:1992
Total airframe hrs:1647 hours
Engine model:Lycoming IO-540-K1G5D
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Waco, TX -   United States of America
Phase: Unknown
Nature:Training
Departure airport:McGregor, TX (PWG)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane had departed the runway and was climbing at 90 knots when the engine/propeller rpm began to over speed. The pilot attempted to adjust the propeller control; however, there was no change in rpm. The airplane lost altitude and impacted trees near the departure end of the runway. Examination of the wreckage revealed that the #6 connecting rod had failed, there was no oil present in the engine, and the oil filter converter plate was missing remnants of its gasket. An Airworthiness Directive (AD) was issued that addressed the oil filter converter plate gasket on engines that had been factory remanufactured after April 1, 1999. The AD required the replacement of the oil filter converter plate gasket before further flight on engines with more than 50 hours time since new, times since overhaul, or time since the last replacement of the gasket or converter plate, and thereafter every 50 hours time in service since the last replacement of the gasket. Non compliance with the AD could result in the protruding or swelling of the converter plate gasket and subsequent loss of engine oil. The engine had been factory remanufactured on May 5, 2000, and had accumulated approximately 376.2 hours since this remanufacture when the accident occurred. Examination of the engine maintenance records revealed that the AD had not been complied with since the engine's remanufacture.
Probable Cause: the mechanic's failure to perform an airworthiness directive, which resulted in the loss of engine oil through a partially failed oil filter converter plate gasket, and subsequent engine failure during takeoff climb. A contributing factor was the lack of suitable terrain for the forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW01LA208
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20010926X01992&key=1

Revision history:

Date/timeContributorUpdates
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
10-Dec-2017 12:55 ASN Update Bot Updated [Other fatalities, Departure airport, Source, Narrative]

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