Accident Morrison E-Racer N345JM,
ASN logo
ASN Wikibase Occurrence # 135016
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 21 June 2008
Time:12:30
Type:Morrison E-Racer
Owner/operator:Private
Registration: N345JM
MSN: 113
Total airframe hrs:365 hours
Engine model:Lycoming IO-360-A1D1
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Aurora, IL -   United States of America
Phase: Take off
Nature:Private
Departure airport:Aurora, IL (ARR)
Destination airport:Urbana, IL (C16)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot experienced a complete loss of engine power during initial climb after takeoff. The airplane was about 1 mile from the airport at 2,000 feet mean sea level at the time. The pilot elected to return to the airport for landing and notified the air traffic control tower accordingly. The cockpit began to fill with smoke, and shortly afterward the pilot reported noticing a fire in the cockpit near the firewall. The pilot successfully continued an approach to the departure runway, intermittently losing visual contact with the runway due to the smoke in the cockpit. On short final, he applied full left aileron and rudder inputs in an attempt to align the airplane for landing; however, the aileron control failed at that time. The airplane landed hard and the left main landing gear collapsed. The airplane spun around and came to rest about 1,500 feet from the runway threshold. The pilot successfully evacuated the airplane, which was subsequently consumed by the fire. The post accident examination was unable to locate the exact source of the fire. The pilot commented that the extent and rapid progression of the fire was consistent with a failure in the high-pressure fuel system.
Probable Cause: An undetermined failure in the high-pressure fuel system, and the subsequent loss of engine power and in-flight fire. Contributing to the accident were the pilot's restricted visibility due to the smoke in the cockpit, failure of the aileron control during landing flare, and the collapse of the left main landing gear due to the hard landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI08LA169
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
03-Dec-2017 11:22 ASN Update Bot Updated [Departure airport, Destination airport, Source, Narrative, Plane category]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org