Accident Mitsubishi MU-2B-20 N310MA,
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ASN Wikibase Occurrence # 136994
 
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Date:Sunday 7 April 1996
Time:11:55 LT
Type:Silhouette image of generic MU2 model; specific model in this crash may look slightly different    
Mitsubishi MU-2B-20
Owner/operator:Ronald C. Bingham
Registration: N310MA
MSN: 167
Year of manufacture:1969
Total airframe hrs:5400 hours
Engine model:Garrett TPE-331-1151A
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Panola County Airport, MS -   United States of America
Phase: Approach
Nature:Private
Departure airport:Montgomery, AL
Destination airport:(0M6)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that loss of power occurred in both engines after he entered the traffic pattern for a full stop landing. The airplane collided with trees during an emergency landing in a cotton field near the airport. Subsequent review of the aircraft maintenance logs disclosed that Mitsubishi MU-2 Service Bulletin (SB) 130A had not been accomplished on this airplane. According to the manufacturer, an inadvertent failure or the improper installation of a filler cap after refueling may cause an air pressure differential between the center and outboard portions of the main integral fuel tank. Air leakage from the filler cap may result in failure of the fuel transfer system to move fuel from the outboard tank section to the center tank section. To eliminate this possible malfunction, the operator was to remove vent check valves from the bulkhead between the tanks in accordance with SB 130A. The operator's maintenance policies required that, company jet and turbo propeller aircraft be maintained under a maintenance program in accordance with FAR Parts 135.415, 135.417, 135.423, 135.443, and a corporate flight management approved aircraft inspection program (AAIP). The maintenance inspection program also included compliance with manufacturers' service bulletins and service letters.

Probable Cause: an anomaly in the fuel system that allowed a pressure differential to occur between the center and outer portions of the main integral fuel tank, which in turn resulted in fuel starvation of both engines. A factor relating to the accident was: failure of company maintenance personnel to remove fuel system vent check valves as recommended by Mitsubishi MU-2 Service Bulletin 130A.

Accident investigation:
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Investigating agency: NTSB
Report number: ATL96LA078
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB ATL96LA078

Location

Revision history:

Date/timeContributorUpdates
06-Mar-2016 22:01 Dr.John Smith Updated [Time, Location, Phase, Departure airport, Destination airport, Source, Narrative]
06-Mar-2016 22:03 Dr.John Smith Updated [Narrative]
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
20-May-2017 18:04 TB Updated [Location, Source, Damage, Narrative]
09-Apr-2024 07:31 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report]

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