ASN Wikibase Occurrence # 137000
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 12 March 1999 |
Time: | 19:00 LT |
Type: | Mitsubishi MU-2B-20 |
Owner/operator: | Gregory K. Benson |
Registration: | N176BJ |
MSN: | 144 |
Year of manufacture: | 1969 |
Total airframe hrs: | 4589 hours |
Engine model: | Garrett 331-1-151 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | McGhee-Tyson Airport, Knoxville, TN -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | (KTYS) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:About 30 minutes into the flight, the right engine lost power. The pilot attempted to restart the engine, but was unsuccessful. The pilot secured the right engine and feathered the right propeller. Shortly after attempting to restart the right engine, the pilot said he also experienced a complete loss of electrical power, and was unable to use his radios. The pilot said he placed the landing gear lever in the down position, and established an approach to runway 5R for an emergency landing. The airplane touched down and skidded off the left side of the runway. Examination of the airplane and the engine assemblies failed to disclose a mechanical malfunction or component failure. During the extensive airplane examination the electrical system was also functionally checked; the examination failed to disclose any mechanical problems. When the master switch was placed in the on position 75% of the battery power was restored to the airplane. The electrical power source was sufficient to activate the landing gear doors. During the examination of the fuel system, fuel was traced from the fuel tank to the fuel control unit. There was no mechanical problems discovered with the right fuel shut-off valve; the right fuel shut-off valve functioned normally.
Probable Cause: A loss of engine power for undetermined reasons. Contributing to the accident was the failure of the landing gear to extend for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL99LA054 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB ATL99LA054
FAA register: FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?omni=Home-N-Number&nNumberTxt=176BJ Location
Revision history:
Date/time | Contributor | Updates |
07-Mar-2016 11:44 |
Dr.John Smith |
Updated [Location, Departure airport, Destination airport, Source, Narrative] |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 10:54 |
ASN Update Bot |
Updated [Departure airport, Destination airport, Source, Narrative] |
20-Sep-2023 06:01 |
Ron Averes |
Updated [[Departure airport, Destination airport, Source, Narrative]] |
08-Apr-2024 08:46 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Departure airport, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation