ASN Wikibase Occurrence # 137077
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Date: | Thursday 30 June 2011 |
Time: | 17:33 |
Type: | Ray Aerial Spraying 773 Racer |
Owner/operator: | Private |
Registration: | N773RY |
MSN: | 001 |
Total airframe hrs: | 2 hours |
Engine model: | Fairchild Ranger V-770 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Ottumwa Regional Airport - KOTM, IA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Ottumwa, IA (OTM) |
Destination airport: | Hedrick, IA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A witness reported that he saw the accident airplane on a crosswind leg for the runway when the nose suddenly went down and the pilot began to maneuver toward the runway. Wreckage path evidence, the location of the initial impact, and a witness statement suggested that the pilot of the amateur-built airplane was making a short, left-hand approach to the runway but had insufficient altitude to reach the paved runway surface. The airplane impacted a berm about 650 feet left of the approach end of the runway, travelled an additional 250 feet, and erupted into flames.
Examination of the airplane’s engine, and ignition system revealed no evidence of a preimpact mechanical malfunction.
Examination of the airplane’s fuel system was not possible due to the extensive fire damage, and no determination of the preimpact condition of the fuel system components could be made. Examination of the airplane’s propeller showed damage consistent with engine rotation with minimal power applied at impact. The witness report, wreckage path evidence, and propeller damage were consistent with an attempt to land the airplane following a loss of engine power.
Probable Cause: The loss of engine power for reasons that could not be determined because postaccident examination of the airplane’s engine and ignition system did not reveal any anomalies that would have precluded normal operation, and extensive postaccident fire damage precluded evaluation of the airplane’s fuel system components.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN11FA436 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
01-Jul-2011 00:50 |
RobertMB |
Added |
01-Jul-2011 08:28 |
RobertMB |
Updated [Aircraft type, Registration, Cn, Operator] |
02-Jul-2011 04:54 |
gerard57 |
Updated [Source, Narrative] |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 16:57 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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