Loss of control Accident Taylorcraft BL-65 N24369,
ASN logo
ASN Wikibase Occurrence # 137761
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Thursday 28 July 2011
Time:15:11
Type:Silhouette image of generic TAYB model; specific model in this crash may look slightly different    
Taylorcraft BL-65
Owner/operator:Private
Registration: N24369
MSN: 1705
Engine model:Lycoming O-145
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:South Oak Aerodrome, Winterville, about 7 miles S. of Greenville, NC -   United States of America
Phase: En route
Nature:Private
Departure airport:Winterville, NC (NC47)
Destination airport:Winterville, NC (NC47)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
After a local flight, the vintage airplane was approaching the pilot's home airport on a very hot day (36 degrees C [97 degrees F]), and the cockpit was most likely hot as well. As the airplane approached perpendicular to the runway, it maintained a nose-down, left bank attitude, consistent with no further control inputs from the pilot. The airplane impacted the left side of runway, approximately one-third down the runway, pivoted 180 degrees, and came to rest about 20 feet from the initial impact point. Examination of the airframe and engine did not reveal evidence of any preimpact mechanical malfunctions. Although the autopsy report listed the cause of death as multiple injuries related to the crash, it also noted significant coronary artery disease and a tiny scar of the papillary muscle. Both suggested the possibility of a cardiac arrhythmia or heart attack that may have resulted in incapacitation. Additionally, the pilot's medical history revealed a vasovagal (fainting) episode due to nausea and vomiting about 2 years prior to the accident. Neither a vasovagal episode nor cardiac arrhythmia would have left any evidence for discovery during autopsy. As such, pilot incapacitation is possible in this accident because of the lack of control inputs as the airplane approached the runway.
Probable Cause: A loss of airplane control for undetermined reasons as the autopsy was unable to reveal any definitive conditions that would have led to the loss of control.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA11FA426
Status: Investigation completed
Duration: 1 year and 8 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
29-Jul-2011 07:56 RobertMB Added
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 17:01 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org