Accident Cessna 172M Skyhawk N5155Q,
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ASN Wikibase Occurrence # 138269
 
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Date:Monday 29 August 2011
Time:14:27
Type:Silhouette image of generic C172 model; specific model in this crash may look slightly different    
Cessna 172M Skyhawk
Owner/operator:Justice Aviation
Registration: N5155Q
MSN: 17261768
Year of manufacture:1973
Total airframe hrs:8227 hours
Engine model:Lycoming O-320-E2D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Near Santa Monica Airport - KSMO, CA -   United States of America
Phase: Approach
Nature:Training
Departure airport:Santa Monica, CA (SMO)
Destination airport:Santa Barbara, CA (SBA)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The student pilot reported that shortly after liftoff, the airspeed indicator needle showed an increase and then a decrease to zero. He realized that the airplane’s airspeed indicator was not operational and advised the air traffic control tower controller. As the pilot returned to land at the airport, the airplane was higher than normal above the runway surface. With a quarter of the runway remaining, the airplane had not touched down. The air traffic control tower controller advised the pilot to go around. The pilot initiated a go-around; however, the airplane impacted trees and a house. The student pilot, as well as his flight instructor, reported that his flight instruction did not include operations simulating a loss of airspeed indication. Although the student pilot reported checking the pitot tube prior to departure, postaccident examination of the airplane’s pitot tube showed that debris, consistent with soil and insect material, was present between the ram air inlet and the drain hole. This resulted in the airspeed indicator showing zero airspeed. Review of the air traffic control services related to the accident revealed that they did not cause or contribute to the accident. The local controller’s actions were reasonable and in accordance with Federal Aviation Administration (FAA) Order 7110.65, “Air Traffic Control”: the local controller handled the situation in accordance with his best judgment based on his perceptions and understanding of the situation.
Probable Cause: The student pilot’s misjudged approach and landing attempt. Contributing to the accident was a lack of airspeed due to a blocked pitot tube.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR11FA415
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
30-Aug-2011 02:25 gerard57 Added
30-Aug-2011 04:54 RobertMB Updated [Time, Aircraft type, Operator, Location, Phase, Departure airport, Destination airport, Source, Narrative]
30-Aug-2011 07:28 RobertMB Updated [Aircraft type, Registration, Cn, Operator, Source, Narrative]
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 17:07 ASN Update Bot Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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