ASN Wikibase Occurrence # 138871
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Date: | Friday 30 September 2011 |
Time: | 13:03 |
Type: | Glasair III |
Owner/operator: | Private |
Registration: | N43KH |
MSN: | 3021 |
Total airframe hrs: | 127 hours |
Engine model: | Chevy LS1 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Falls of Rough, KY -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Rough River State Park Airport, KY (2I3) |
Destination airport: | Rough River State Park Airport, KY (2I3) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to witnesses, the airplane departed the airport and circled back to make a fly-by over the runway. As the airplane flew over the runway, a witness reported that the engine sounded like it “over revved.” Witnesses also stated that they saw what appeared to be a puff of smoke emitting from the nose of the airplane. The pilot made a left banking turn, and then entered a left downwind for the runway. The engine power seemed to surge as the airplane descended. Then the engine went silent and the airplane turned toward the airport but did not have enough altitude to reach the runway. The pilot appeared to level the wings, and the landing gear was lowered as the airplane descended into the trees, struck a building, and exploded.
A postaccident examination of the airplane revealed that it was equipped an automotive Chevrolet LS1 engine. The airplane’s propeller was attached to a propeller speed reduction unit (PSRU). The system was designed with an automatic clutch and was tuned to remain disengaged at idle and engage with an increase in power. An examination of the PSRU revealed that the propeller drive shaft fractured as a result of fatigue. This fracture separated the propeller drive gears from the clutch, which resulted in the loss of power to the propeller. Given the witness accounts of the loss of engine power, it is likely that the airplane lost airspeed and altitude due to this condition.
Probable Cause: The failure of the propeller power speed reduction unit, which resulted in a loss of engine power at low altitude.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA11FA512 |
Status: | Investigation completed |
Duration: | 1 year and 9 months |
Download report: | Final report |
|
Sources:
NTSB
http://www.nbcnews.com/id/44733966/ns/us_news-life/t/plane-crashes-motel-near-kentucky-state-park/#.XGjInqJKjDc Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
30-Sep-2011 14:11 |
gerard57 |
Added |
30-Sep-2011 14:34 |
gerard57 |
Updated [Other fatalities, Source, Narrative] |
01-Oct-2011 01:17 |
Geno |
Updated [Location, Source] |
01-Oct-2011 02:00 |
RobertMB |
Updated [Aircraft type, Location, Departure airport, Source, Narrative] |
01-Oct-2011 11:36 |
harro |
Updated [Time, Narrative] |
01-Oct-2011 18:30 |
RobertMB |
Updated [Time, Aircraft type, Registration, Cn, Operator, Phase, Departure airport, Source, Narrative] |
10-Oct-2011 22:04 |
Geno |
Updated [Departure airport, Source, Narrative] |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 17:15 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
17-Feb-2019 07:35 |
jasonmaky |
Updated [Source] |
17-Feb-2019 07:36 |
harro |
Updated [Other fatalities, Source, Photo, Accident report, ] |
13-Mar-2022 04:49 |
Captain Adam |
Updated [Location, Departure airport, Destination airport, Source, Narrative, Photo] |
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