ASN Wikibase Occurrence # 144730
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 30 March 2012 |
Time: | 17:30 |
Type: | Hughes 500D (369D) |
Owner/operator: | Dah Aircraft Llc |
Registration: | N868W |
MSN: | 1000800D |
Year of manufacture: | 1980 |
Total airframe hrs: | 17804 hours |
Engine model: | Rolls Royce 250-C20B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near South Mine Street, McCormick, SC -
United States of America
|
Phase: | En route |
Nature: | Ferry/positioning |
Departure airport: | Mccormick, SC |
Destination airport: | Aiken, SC (AIK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was en route to his destination airport and had not obtained a weather briefing. A weather front came through, and the wind changed from a tailwind to a headwind, so he could not reach is destination and diverted to an alternate airport to refuel. However, he landed at the wrong airport, and that airport did not have any Jet A fuel. He observed an automotive gas station and flew to it and landed in the grass nearby, even though he did not know what the approved alternate fuel was for the turbine engine. He purchased 25 gallons of 87 octane automotive fuel and placed it in the helicopter’s fuel tank. According to the engine manufacturer, automotive fuel is not an approved fuel on the list. He started the engine and departed. He was about 150 to 200 feet above the ground when the engine lost power. The engine-out audio and low-rpm audio sounded. He lowered the collective pitch as much as possible to clear a power line and reach an open field. Once clear of the power line, he lowered the collective pitch to the full-down position. The helicopter touched down hard in a tail-low attitude. The nose pitched downward, the tail boom separated, and the helicopter slid forward and rolled over on its right side. No preaccident mechanical malfunctions or failures were found that would have precluded normal operation.
Probable Cause: The pilot's decision to use automotive fuel instead of the approved alternate fuel, which resulted in a total loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12LA260 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
31-Mar-2012 07:01 |
gerard57 |
Added |
31-Mar-2012 07:49 |
RobertMB |
Updated [Time, Aircraft type, Registration, Cn, Operator, Location, Departure airport, Destination airport, Source, Narrative] |
10-Apr-2012 11:53 |
Geno |
Updated [Time, Operator, Departure airport, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:26 |
ASN Update Bot |
Updated [Cn, Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation