Loss of control Accident Beechcraft A36TC Bonanza N2WZ,
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ASN Wikibase Occurrence # 145639
 
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Date:Saturday 12 May 2012
Time:12:45
Type:Silhouette image of generic BT36 model; specific model in this crash may look slightly different    
Beechcraft A36TC Bonanza
Owner/operator:L & M Trucking
Registration: N2WZ
MSN: EA-174
Year of manufacture:1980
Total airframe hrs:5158 hours
Engine model:Continental. TSIO-520
Fatalities:Fatalities: 0 / Occupants: 6
Aircraft damage: Substantial
Category:Accident
Location:Harnett Regional Jetport Airport - KHRJ, Erwin, NC -   United States of America
Phase: Take off
Nature:Private
Departure airport:Erwin, NC (HRJ)
Destination airport:Darlington, SC (UDG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
After what he described as an uneventful engine run-up, the pilot took off from the 5,000-foot-long runway. The pilot stated that when the airplane reached an altitude of about 50 feet, he retracted the landing gear; the engine lost partial power. The airplane yawed to the left and touched down again, impacting a thicket. According to a witness who observed the takeoff, the engine power never decreased until the engine stopped suddenly upon impacting the ground.

Postaccident examination of the engine revealed that the No. 4 cylinder exhaust valve springs had fractured in fatigue. Detailed examination of the springs showed that the fatigue cracking likely originated from one or more of the iron oxide (rust) pits present on the surface of the springs. The springs had been installed in the engine about 1 year before the accident flight. According to the mechanic who installed the springs, he had retrieved them from a similar engine’s cylinder that was removed from another airplane; there was no documentation of the springs’ service history or serviceability.
Probable Cause: The partial loss of engine power shortly after takeoff due to fatigue-fractured exhaust valve springs. Contributing to the accident was the mechanic’s decision to install exhaust valve springs with an unknown service history in the engine’s No. 4 cylinder.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA12LA336
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB

History of this aircraft

Other occurrences involving this aircraft
7 February 1981 N2WZ Private 0 Scotts Valey Airport, California (SKYPARK) w/o

Location

Revision history:

Date/timeContributorUpdates
15-May-2012 10:24 Geno Added
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 20:40 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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