ASN Wikibase Occurrence # 14663
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Date: | Tuesday 12 February 2008 |
Time: | 15:05 |
Type: | Beechcraft A45 Mentor |
Owner/operator: | Goldwing Aviation, LLC |
Registration: | N34KF |
MSN: | G-120 |
Total airframe hrs: | 7847 hours |
Engine model: | Continental IO-520 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Englewood, CO -
United States of America
|
Phase: | Initial climb |
Nature: | Executive |
Departure airport: | Englewood, CO (APA) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that the airplane the battery was dead, and he used an external source to "charge/start the airplane." The taxi and initial takeoff were uneventful. During the landing gear retraction after takeoff, the airplane "lost total electrical power." The pilot elected to continue the flight and troubleshoot the electrical failure. With no electrical power, the pilot had no communications, and had to manually extend the landing gear. A second airplane flew near the accident airplane to help verify that the landing gear was extended. The landing gear appeared to be extended, and the pilot attempted to land the airplane. During the landing roll, the right main landing gear collapsed and the airplane went off the runway. The right wing impacted a runway sign, and the nose landing gear and left main landing gear collapsed. The airplane came to rest upright approximately 10 feet off the runway. An examination of the airplane showed that the aircraft battery was completely discharged. The owner of the airplane reported that the alternator would not be able to handle the electrical load during landing gear retraction without battery power.
Probable Cause: The pilot's improper decision to fly the airplane with a discharged battery, which resulted in a total electrical failure during takeoff climb. Contributing factors were the pilot's inability to verify the landing gear position, and the impact with the runway sign.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN08LA057 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
ex.USAF/53-3359.
Location
Revision history:
Date/time | Contributor | Updates |
25-Feb-2008 22:17 |
Circeus |
Added |
20-Oct-2008 00:49 |
RobertMB |
Updated |
28-Jun-2016 19:09 |
TB |
Updated [Aircraft type, Nature, Source, Damage] |
21-Dec-2016 19:13 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 09:34 |
ASN Update Bot |
Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
08-Feb-2022 14:05 |
A.J.Scholten |
Updated [Source] |
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