ASN Wikibase Occurrence # 146677
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 7 July 2012 |
Time: | 14:38 |
Type: | Boeing/Jones 75 |
Owner/operator: | Private |
Registration: | N3993P |
MSN: | AR-33 |
Total airframe hrs: | 855 hours |
Engine model: | Continental W670 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bayport Aerodrome Bayport - 23N, NY -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Bayport, NY (23N) |
Destination airport: | Bayport, NY (23N) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he had conducted six previous uneventful flights on the day of the accident utilizing both runways 18 and 36 for takeoff due to variable winds. He elected to depart from runway 18 on the accident flight, because the windsock indicated a primarily southwesterly wind. The pilot stated that the takeoff roll was normal; however, shortly after liftoff, the airplane encountered a tailwind, which resulted in a degradation of performance. The airplane began to sink and lose airspeed, and the pilot aborted the takeoff. The airplane touched back down onto the runway, and the pilot applied the brakes in an effort to stop the airplane on the remaining runway. The airplane nosed over, which resulted in substantial damage to the vertical stabilizer. The pilot, pilot-rated passenger, and several witnesses reported a wind shift around the time of the accident. Weather reports from a nearby airport revealed that, during the period from about 1 hour 40 minutes before to about 20 minutes after the accident, there was a 40 degree shift in wind direction and an increase in wind speed from 9 knots to 18 knots, gusting to 24 knots. Postaccident examination of the airplane revealed no mechanical anomalies that would have precluded normal operation.
Probable Cause: The airplane’s encounter with a wind shift to a tailwind during takeoff, which resulted in the pilot’s decision to abort the takeoff and the airplane’s subsequent runway overrun.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12CA434 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register: [LINK NOT WORKING ANYMORE:http://nycaviation.com/forum/threads/43644-Plane-flips-at-Bayport-Aerodrome-2-hurt]
http://abclocal.go.com/wabc/story?section=news/local/long_island&id=8728818 https://patch.com/new-york/sayville/small-plane-crashes-at-bayport-aerodome http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=3993P http://jetphotos.net/viewphoto.php?id=7240648&nseq=0 Location
Revision history:
Date/time | Contributor | Updates |
09-Jul-2012 18:03 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:55 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation