Loss of control Accident Cozy III N718JT,
ASN logo
ASN Wikibase Occurrence # 146704
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Wednesday 11 July 2012
Time:12:40
Type:Silhouette image of generic COZY model; specific model in this crash may look slightly different    
Cozy III
Owner/operator:Private
Registration: N718JT
MSN: BUNCH 1
Engine model:Lycoming O-320
Fatalities:Fatalities: 1 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Winslow-Lindbergh Regional Airport - KINW, Winslow, AZ -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Winslow, AZ (INW)
Destination airport:Denver, CA (DEN)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that, during takeoff, the airplane became airborne with 3,000 ft of runway remaining. When the airplane was between about 25 and 40 ft above ground level (agl), its nose dropped, and the pilot then pulled back on the control stick. The pilot was able to level out the airplane and establish a 200-ft-per-minute climb rate. As the airplane approached 75 ft agl at an indicated airspeed of about 95 mph, the airplane’s nose dropped to about a 30- to 45-degree nose-down attitude. The pilot again pulled back on the control stick, but he was unable to regain control of the airplane before it impacted the ground.
The pilot reported that the engine was running roughly during an initial start-up, but he stated that it ran normally during a subsequent start-up and two engine run-ups before taking off on the accident flight. A postaccident examination of the engine and airframe revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. The airplane’s calculated gross weight exceeded its allowable maximum gross weight, and high-density altitude conditions existed at the time of the accident. Although these conditions likely affected the airplane’s performance, the pilot was able to establish a positive climb rate after takeoff; however, he did not maintain control of the airplane as the pitch changed.


Probable Cause: The pilot’s failure to maintain airplane control during climb in high-density altitude conditions and with the airplane’s weight in excess of its maximum allowable gross weight.


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR12LA302
Status: Investigation completed
Duration: 2 years and 6 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
12-Jul-2012 05:48 78Delta Added
12-Jul-2012 05:49 harro Updated [Date, Aircraft type]
12-Jul-2012 08:02 Geno Updated [Time, Aircraft type, Operator, Location, Source, Narrative]
12-Jul-2012 08:10 Geno Updated [Source]
13-Jul-2012 15:58 Geno Updated [Source]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 20:56 ASN Update Bot Updated [Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org