Runway excursion Accident Van's RV-7A N404JT,
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ASN Wikibase Occurrence # 146723
 
This record has been locked for editing.

Date:Saturday 14 July 2012
Time:16:00
Type:Silhouette image of generic RV7 model; specific model in this crash may look slightly different    
Van's RV-7A
Owner/operator:Private
Registration: N404JT
MSN: 71352
Year of manufacture:2007
Total airframe hrs:289 hours
Engine model:Superior SL-IO-360-B1C
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Novato, CA (KDVO) -   United States of America
Phase: Approach
Nature:Private
Departure airport:Novato, CA (DVO)
Destination airport:Novato, CA (DVO)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that, during the takeoff climb, he reduced the engine power setting and that, shortly after, the engine did not respond, and he noted that the engine manifold pressure was 5 inches. The pilot attempted to troubleshoot the problem by adjusting the throttle and mixture controls without success. He chose to return to the airport for a precautionary landing; however, he was unsure if the airplane could reach the active runway, so he then chose to land on the closest runway with a 6- to 9-knot tailwind. Due to excessive altitude and airspeed for landing on that runway, the pilot did not use flaps and attempted a forward slip. The airspeed continued to increase during the descent, and the airplane landed midway down the runway. The airplane subsequently overran the runway end, traversed a ditch, and came to rest inverted. If the pilot had been able to control the slip to reduce the altitude and airspeed, he might have been able to land the airplane at a point on the runway with adequate distance to stop it. Postaccident engine examination revealed no mechanical malfunctions or failures that would have precluded normal operation.

Probable Cause: The partial loss of engine power for reasons that could not be determined because postaccident examination revealed no mechanical malfunctions or failures that would have precluded normal operation. Contributing to the accident was the pilot’s failure to control a forward slip to reduce the altitude and airspeed to attain a proper touchdown point during landing.
 

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR12LA321
Status: Investigation completed
Duration: 3 years and 3 months
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=404JT

Location

Revision history:

Date/timeContributorUpdates
14-Jul-2012 23:16 Geno Added
15-Jul-2012 14:11 harro Updated [Aircraft type, Narrative]
16-Jul-2012 04:46 gerard57 Updated [Aircraft type, Damage]
05-Sep-2016 04:13 junior sjc Updated [Narrative]
07-Sep-2016 06:13 junior sjc Updated [Narrative]
07-Sep-2016 07:30 junior sjc Updated [Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
05-Nov-2017 08:28 junior sjc Updated [Location, Destination airport, Narrative]
27-Nov-2017 20:54 ASN Update Bot Updated [Aircraft type, Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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