ASN Wikibase Occurrence # 146930
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Date: | Tuesday 24 July 2012 |
Time: | 19:00 |
Type: | Hughes 269C |
Owner/operator: | Private |
Registration: | N9679F |
MSN: | 310103 |
Year of manufacture: | 1971 |
Total airframe hrs: | 2393 hours |
Engine model: | Lycoming HIO-360-D1A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | 4550 35th Street North, Lealman, St. Petersburg, FL -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | St. Petersburg, FL |
Destination airport: | St. Petersburg, FL |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, the helicopter's last annual inspection had been completed 12 years prior to the accident. On the day of the accident, he decided to fly it to lubricate the parts. After liftoff, he brought the helicopter to a hover about 25 feet in the air and initiated some pedal turns. The nose of the helicopter then began to drift toward the right. He applied left pedal but the helicopter didn’t respond. The helicopter then circled 6 to 8 times, so the pilot lowered the collective, and the helicopter impacted the ground on the left skid, struck a fence, and then rolled over on its left side.
However, according to witnesses, the helicopter was about 50 feet in the air, did not circle but moved side to side, and was described as being out of control before it impacted the ground. Total flight time from liftoff to impact was about 2 minutes in duration. Postaccident examination did not reveal any preimpact failures or malfunctions of the helicopter which would have precluded normal operation. However, the cyclic control system would not move freely because the lateral friction control was tightened down. Once the lateral friction control was released, lateral movement of the cyclic control was possible.
Probable Cause: The pilot's failure to assure that the lateral friction control was released prior to flight.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12LA477 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB
FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=9679F Location
Revision history:
Date/time | Contributor | Updates |
25-Jul-2012 23:03 |
Geno |
Added |
13-Feb-2016 20:20 |
Dr.John Smith |
Updated [Time, Operator, Location, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:57 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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