Accident Mooney M20TN Acclaim N411JL,
ASN logo
ASN Wikibase Occurrence # 147218
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Friday 27 July 2012
Time:08:46
Type:Silhouette image of generic M20T model; specific model in this crash may look slightly different    
Mooney M20TN Acclaim
Owner/operator:4th Wave Inc.
Registration: N411JL
MSN: 31-0096
Total airframe hrs:594 hours
Engine model:Continental TSIO-550-G1
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Lenawee County Airport - KADG, Adrian, MI -   United States of America
Phase: Landing
Nature:Private
Departure airport:Oshkosh, WI (OSH)
Destination airport:Manassas, VA (HEF)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that the airplane, with its autopilot engaged, experienced a “violent pitch-up” without warning while it was climbing through about flight level 180. Extreme forward yoke pressure (the pilot estimated between 100 and 150 pounds force) was required to keep the airplane from pitching up and stalling, so the pilot kept both hands on the yoke.
The Airplane Flight Manual contains emergency procedures for use in the event of an autopilot out-of-trim event; the third item on the checklist directs pilots to re-trim the pitch, if necessary, using the trim wheel. The pilot noted that he did not attempt to use the manual trim wheel to change the airplane’s pitch attitude because that would have required him to release hand pressure on the control yoke. He was uncertain when or how the autopilot was disengaged. He declared an emergency and made a spiraling descent to lose altitude. He reported that he encountered multiple violent pitch up and down oscillations near the bottom of the descent; the pilot’s seat was broken during one of the oscillations, which allowed the pilot to use his knees to apply forward yoke pressure. He stated that by using his knees to control the yoke, the airplane was “quasi-stable,” pitch oscillations still occurred due to the lack of precise pitch control. While still having difficulty controlling the airplane’s pitch with the electric nose pitch trim in the full up position, he prepared for an emergency landing. The pilot used his knees to provide forward yoke pressure as he landed the airplane about 450 feet short of the runway. The airplane’s nose gear collapsed, the main landing gear were sheared off, and the airplane skidded about 900 feet before coming to rest to the left of the runway. The duration of the flight from the initial pitch up event to landing was about 27 minutes. Three separate examinations of the airplane’s flight controls and autopilot system found no anomalies with the autopilot system or an explanation for the violent nose-pitch-up event. The Emergency Section of the Airplane Flight Manual (AFM) supplement for the autopilot stated that for an Autopilot Out of Trim emergency the pilot should: 1) disengage the autopilot 2) maintain/regain aircraft control, and 3) pitch trim...re-trim if necessary using the trim wheel.
   



Probable Cause: An initial nose-pitch-up event and out-of-trim condition, the reason for which could not be determined because the examinations of the airplane did not reveal any anomalies that would have precluded normal operation. Contributing to the accident was the pilot’s failure to use the manual trim wheel to reset the pitch trim. 


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN12FA487
Status: Investigation completed
Duration: 2 years and 2 months
Download report: Final report

Sources:

NTSB
http://web.archive.org/web/20120731000025/http://www.lenconnect.com:80/news/police_and_fire/x2095084651/Pilot-makes-emergency-landing-at-Lenawee-County-Airport
https://www.faa.gov/data_research/accident_incident/preliminary_data/events01/media/01_411JL.txt

http://www.airport-data.com/aircraft/N411JL.html
https://flightaware.com/live/flight/N411JL

History of this aircraft

Other occurrences involving this aircraft
20 June 2009 N411JL 4th Wave Inc. 0 San Jose, CA sub
Bounced on landing

Location

Revision history:

Date/timeContributorUpdates
30-Jul-2012 09:11 Geno Added
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
27-Nov-2017 20:55 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org