ASN Wikibase Occurrence # 149226
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Date: | Monday 10 September 2012 |
Time: | 11:00 |
Type: | Wiggins Air Boss |
Owner/operator: | Private |
Registration: | N717EW |
MSN: | 001 |
Year of manufacture: | 2012 |
Total airframe hrs: | 1 hours |
Engine model: | Subaru EJ22 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Lansing Municipal Airport - KIGQ, Lansing, IL -
United States of America
|
Phase: | Take off |
Nature: | Test |
Departure airport: | Lansing, IL (IGQ) |
Destination airport: | Lansing, IL (IGQ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The accident occurred during a flight test of the experimental gyroplane. A witness reported seeing the gyroplane yaw nose left and roll right shortly after liftoff. The gyroplane then descended briefly before it rolled back to level and entered a climb. The gyroplane climbed to about 100 feet above the ground while continuing to fly on the runway heading before it yawed nose left again, entered a right roll, and descended rapidly into a cornfield south of the runway. Another witness reported that he heard the gyroplane's engine running until the gyroplane impacted terrain. No preimpact mechanical malfunctions or anomalies were found that would have precluded normal operation of the gyroplane.
The private pilot did not possess a rotorcraft rating; however, federal aviation regulations allow certificated pilots to operate experimental aircraft without an applicable category or class rating. A gyroplane flight instructor reported that he had provided the pilot 1.8 hours of familiarization training in another gyroplane more than 3 months before the accident. He added that the accident pilot told him that he had not flown in over 20 years. Additionally, no record was found indicating that the pilot received any flight training in gyroplanes subsequent to the familiarization training. It is likely that the pilot's overall lack of familiarity with the operation of gyroplanes resulted in his failure to maintain control during the accident flight.
Probable Cause: The pilot's failure to obtain adequate familiarization with gyroplane operations before attempting a flight test of the recently completed gyroplane, which resulted in his failure to maintain control during the accident flight.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN12FA619 |
Status: | Investigation completed |
Duration: | 2 years |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=717EW&x=0&y=0 Location
Revision history:
Date/time | Contributor | Updates |
19-Sep-2012 13:41 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
28-Nov-2017 13:26 |
ASN Update Bot |
Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Plane category] |
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