Accident Beechcraft A36 Bonanza N517DJ,
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ASN Wikibase Occurrence # 157544
 
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Date:Wednesday 10 July 2013
Time:04:45
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36 Bonanza
Owner/operator:Silver Sage Aviation
Registration: N517DJ
MSN: E-3075
Year of manufacture:1997
Total airframe hrs:1294 hours
Engine model:Continental IO-550 SERIES
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Near Fallon Municipal Airport (KFLX), Fallon, NV -   United States of America
Phase: Take off
Nature:Passenger - Non-Scheduled/charter/Air Taxi
Departure airport:Fallon, NV (FLX)
Destination airport:Dixie Vally, NV (NV30)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that, during climbout, when the airplane was about 1,000 ft above ground level, the engine lost power. The pilot subsequently maneuvered the airplane to attempt to land on the departure runway. The airplane touched down short of the runway in rough, desert terrain, which resulted in substantial damage to the wings, fuselage, and empennage.
A postaccident engine examination revealed that the No. 5 connecting rod cap and one of its two bolts had fractured midlength; the opposite bolt was intact with the nut still fastened. Metallurgical examination revealed that the No. 5 connecting rod had failed due to a fatigue crack that had initiated on the outer surface of the nut-facing boss. The crack propagated inward until the final cross-section of the connecting rod yoke failed in overstress, which then catastrophically breeched the left side of the engine case. The fatigue crack did not show any material imperfections; however, the surface finish of the boss where the fatigue crack initiated was consistent with it having been shot peened. Although shot peening is performed to impart compressive stresses to prevent fatigue crack initiation, excessive peening times may sufficiently alter the surface to create stress concentrators. However, the configuration of the fractured rod yoke precluded any accurate surface roughness measurements and, therefore, it could not be determined if improper surface modification had occurred.
 

Probable Cause: A fatigue failure of the No. 5 connecting rod, which resulted in a catastrophic engine failure during the initial climb and a subsequent forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR13LA321
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=517DJ

Location

Revision history:

Date/timeContributorUpdates
10-Jul-2013 19:08 Geno Added
10-Jul-2013 19:44 RobertMB Updated [Registration, Cn, Source]
12-Jul-2013 14:10 Anon. Updated [Nature, Damage]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
29-Nov-2017 08:50 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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