ASN Wikibase Occurrence # 158773
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Date: | Tuesday 20 August 2013 |
Time: | 14:54 |
Type: | Beechcraft C23 Sundowner |
Owner/operator: | Private |
Registration: | N243RG |
MSN: | M-2150 |
Year of manufacture: | 1979 |
Total airframe hrs: | 3676 hours |
Engine model: | Lycoming O-360-A4K |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Gadabout Gaddis Airport (ME08), Bingham, ME -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Bingham, ME (ME08) |
Destination airport: | Augusta, ME (AUG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane had arrived at the departure airport earlier in the day. Witnesses, including the passenger, stated that it took multiple attempts for the pilot to land on the turf runway upon arrival; however, the pilot reported that “it was a non-event going in.” The airplane subsequently took off from the 2,000-ft-long, turf-covered runway that had trees near its departure end. The pilot reported that, during takeoff, the airspeed indicator did not appear to be working, so he “tapped it” with his fingers. He estimated that the airplane was traveling about 60 to 70 mph at that time. He pulled back on the control wheel, and, when the airplane reached about 20 ft above ground level, the stall warning activated. He then pushed forward on the control wheel to gain airspeed and turned the airplane slightly upriver. The right wing then contacted trees, and the airplane subsequently impacted the river nose first. Examination of the wreckage did not reveal any evidence of preimpact failures or malfunctions of the airplane or engine that would have precluded normal operation.
At the time of the accident, the temperature was about 80 degrees F, and the calculated density altitude was about 3,218 ft, which would have decreased the airplane’s climb rate by about 30 percent. Further, according to the airplane flight manual, about 2,300 ft of turf runway would have been needed to clear a 50-ft obstacle. Therefore, due to the extended required ground roll and the degraded climb performance, the airplane was likely not able to attain a sufficient climb rate to clear the trees at the end of the runway.
Probable Cause: The pilot's inadequate preflight planning, which resulted in his attempt to take off from a short, turf runway in high-density altitude conditions under which the airplane was unable to attain a positive climb rate to clear trees.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA13LA370 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Media:
Revision history:
Date/time | Contributor | Updates |
21-Aug-2013 08:55 |
harro |
Added |
21-Aug-2013 19:00 |
Geno |
Updated [Operator, Location, Departure airport, Destination airport, Source, Embed code, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 09:00 |
ASN Update Bot |
Updated [Registration, Operator, Other fatalities, Departure airport, Destination airport, Source, Embed code, Narrative] |
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