Accident Bellanca 8KCAB Decathlon N413JJ,
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ASN Wikibase Occurrence # 159396
 
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Date:Tuesday 27 August 2013
Time:17:08
Type:Silhouette image of generic BL8 model; specific model in this crash may look slightly different    
Bellanca 8KCAB Decathlon
Owner/operator:Private
Registration: N413JJ
MSN: 1092-2009
Year of manufacture:2009
Total airframe hrs:840 hours
Engine model:Lycoming AEIO 360 41B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:near Wheeler AAF, Oahu, HI -   United States of America
Phase: En route
Nature:Private
Departure airport:Honolulu-Daniel K. Inouye International Airport, HI (HNL/PHNL)
Destination airport:Honolulu-Daniel K. Inouye International Airport, HI (HNL/PHNL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that, shortly after he completed an aerobatic maneuver and while the airplane was in cruise flight about 4,000 ft above ground level, the engine lost power. The pilot initiated a turn back toward the nearest airport. When he realized that the airplane would be unable to reach the airport, he initiated a forced landing in a field. During the landing roll, the airplane nosed over and then came to rest inverted. Postaccident examination of the airplane the following day revealed that there was fuel in the header tank, but the quantity of fuel in the main tanks could not be determined because the airplane was inverted. Several days after the accident and during the airplane recovery, a small amount of fuel was observed in each main tank. It could not be determined if fuel had leaked from the tanks while the airplane was inverted. A postaccident examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. The engine was test run at various power settings with no anomalies noted.

Probable Cause: A total loss of engine power during cruise flight for reasons that could not be determined because postaccident examination of the engine and airframe did not reveal any anomalies that would have precluded normal operation.


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR13LA389
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=413JJ

Location

Revision history:

Date/timeContributorUpdates
28-Aug-2013 13:00 gerard57 Added
29-Aug-2013 03:28 Geno Updated [Time, Aircraft type, Registration, Cn, Location, Phase, Nature, Source, Damage, Narrative, Plane category]
30-Aug-2013 06:12 Anon. Updated [Registration]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
29-Nov-2017 08:58 ASN Update Bot Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]
10-Jun-2023 16:09 Ron Averes Updated [[Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]]

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