Accident Piper PA-32R-300 Cherokee Lance N5605V,
ASN logo
ASN Wikibase Occurrence # 161443
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Monday 14 October 2013
Time:17:00
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R-300 Cherokee Lance
Owner/operator:Baxter Flying Inc
Registration: N5605V
MSN: 32R-7780346
Year of manufacture:1977
Total airframe hrs:6948 hours
Engine model:Lycoming IO-540 K1G5D
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Pope County, near Hector, AR -   United States of America
Phase: Landing
Nature:Private
Departure airport:Fayetteville, AR (KFYV)
Destination airport:Tunica, MS (KUTA)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that, during climbout, he noticed that the engine was vibrating. After leveling off the airplane, the vibration worsened, and the engine subsequently experienced a total loss of power. The pilot executed a forced landing onto a road, and the airplane impacted a fence post.
Examination of the engine revealed that the crankshaft was fractured through the No. 8 cheek position between the Nos. 5 and 6 pistons. Fatigue cracking emanated from the connecting rod journal where the No. 5 connecting rod mates. The No. 6 piston cooling nozzle was not found in its position, and its pieces were found in the bottom of the sump; the pieces were more intact than would be expected if they had been ground between the crankshaft and connecting rod for an appreciable amount of time. Also, there was no evidence of a gouge or other mechanical damage on the No. 5 connecting rod journal. Based on this evidence, it is unlikely that the fatigue cracking was initiated by the No. 6 cooling nozzle being lodged against the crankshaft after falling out of position.
About 18 months before the accident, the engine was repaired and overhauled due to a propeller strike. Further, about 4 months before the accident, maintenance personnel performed a top overhaul of the engine, and, about 1 month before the accident, maintenance personnel replaced the No. 2 cylinder. The timing of the failure suggests that an imbalance could have been introduced to the engine during one or both of the maintenance procedures, which could have resulted in the initiation of the fatigue cracking and the subsequent falling out of the No. 6 cooling nozzle; however, the exact cause of the crankshaft fatigue cracking could not be determined.

Probable Cause: An engine failure due to crankshaft fatigue cracking for reasons that could not be determined based on the available evidence.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN14LA030
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
https://flightaware.com/live/flight/N5605V

FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=5605V

Location

Revision history:

Date/timeContributorUpdates
15-Oct-2013 01:00 Geno Added
15-Oct-2013 01:09 Geno Updated [Source, Damage, Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
29-Nov-2017 09:17 ASN Update Bot Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org