ASN Wikibase Occurrence # 162544
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Date: | Thursday 28 November 2013 |
Time: | 09:50 |
Type: | Beechcraft V35 Bonanza |
Owner/operator: | Private |
Registration: | N5655D |
MSN: | D-8406 |
Year of manufacture: | 1967 |
Total airframe hrs: | 7080 hours |
Engine model: | Continental IO-550 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Birmingham-Shuttlesworth Int'l Airport (KBHM), Birmingham, AL -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Norfolk, VA (ORF) |
Destination airport: | Birmingham, AL (BHM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, during approach, he heard a “loud pop” and that the engine then lost total power. The airplane was too far away to glide to the destination airport, so the pilot chose to perform a forced landing to a field, which resulted in substantial damage to the fuselage.
Subsequent teardown examination of the engine revealed evidence of oil starvation at the No. 2 connecting rod, which resulted in its separation from the crankshaft and its subsequent puncturing of a hole in the crankcase. The oil tube from the main bearing to the No. 2 connecting rod was found clear and unrestricted. At some point during the life of the engine, the interior of the rocker covers had been coated with an unapproved material. The coating material had been flaking off during operation and had been cleaned from two of six of the rocker covers. The four remaining covers still contained the coating material, but it could not be determined if the material caused the oil restriction because none of the material was found in any of the oil or oil passages. However, it is possible that any restricting material dislodged and escaped during the engine failure.
Probable Cause: The failure of the No. 2 connecting rod due to oil starvation, which resulted in a total loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA14LA052 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=5655D https://flightaware.com/live/flight/N5655D Location
Revision history:
Date/time | Contributor | Updates |
28-Nov-2013 19:29 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 09:23 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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