ASN Wikibase Occurrence # 162981
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Date: | Monday 16 December 2013 |
Time: | 21:15 |
Type: | Cessna 182T Skylane |
Owner/operator: | Civil Air Patrol |
Registration: | N963CP |
MSN: | 18281973 |
Year of manufacture: | 2007 |
Total airframe hrs: | 1703 hours |
Engine model: | Lycoming IO-540-AB1A5 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Burlington-Alamance Airport, NC -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Burlington Alamance Regional Airport, NC (KBUY) |
Destination airport: | Bunbury Airport, WA (BUY/YBUN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he was practicing night takeoffs and landings. He completed two takeoffs and landings without incident; however, during the third takeoff, as the airplane was climbing to between about 10 and 20 ft above ground level, it stopped climbing, and the pilot felt increased resistance on the elevator control. The airplane did not respond to elevator control inputs, and it subsequently pitched nose down and descended. The airplane touched down before departing the left side of the runway. The nose gear collapsed, and the airplane sustained substantial damage to the firewall and nose section.
The pilot reported that the airplane had a recent history of elevator trim issues, which included difficulty controlling the elevator. The elevator trim jackscrew had been removed, inspected, and reinstalled about 1 week before the accident, and the airplane had since been operated about 7 hours. Examination of the airplane, including the elevator control system, did not reveal any preimpact mechanical malfunctions that would have precluded normal operation; however, impact damage precluded the ability to conduct a complete functional check of the elevator control system.
Probable Cause: A loss of airplane control during takeoff for reasons that could not be determined due to the postaccident condition of the elevator control system.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA14LA072 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
02-Jan-2014 22:52 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 09:27 |
ASN Update Bot |
Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
31-May-2023 13:33 |
Ron Averes |
Updated [[Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]] |
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