ASN Wikibase Occurrence # 164493
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 5 March 2014 |
Time: | 10:56 |
Type: | Cessna 172R Skyhawk |
Owner/operator: | Private |
Registration: | N9417Z |
MSN: | 17280265 |
Year of manufacture: | 1997 |
Total airframe hrs: | 4083 hours |
Engine model: | Lycoming I0-360-B1E |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Mc Kellar-Sipes Regional Airport (KMKL), Jackson, TN -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Jackson, MS (MKL) |
Destination airport: | Augusta, GA (AGS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, during the climb after takeoff in instrument meteorological conditions, he noted that the engine was losing oil pressure rapidly. He immediately made a 180-degree turn to return to the departure airport. While inbound on the instrument landing system (ILS) approach, he realized that the airplane was too high, so he executed a 360-degree descending turn. He then again proceeded inbound on the ILS approach. He continued the descent but, because the airplane had not captured the glideslope, he executed a missed approach. He then circled the airplane around and re-established the airplane on the localizer. Subsequently, the engine lost all power, and the airplane began descending. The pilot subsequently landed the airplane on a road just north of the airport. During the landing, the right wing impacted a highway sign, which resulted in substantial damage to the right wing. The airplane then veered right and entered a cornfield.
Examination of the wreckage revealed the presence of oil on the back of the engine, firewall, and belly. The engine was started with the engine cowling removed, and oil was observed to appear on the back of the accessory pad near the lower vacuum pump. Further examination of the area revealed that the accessory drive adapter gasket was the source of the leak. Review of the airplane’s maintenance records revealed that, on the day before the accident, the lower vacuum pump had been removed and that a new vacuum pump, shaft seal, and accessory drive adapter gasket had been installed. Examination revealed that the proper gasket was installed; however, it was distorted and showed signs of excessive compression and “squeezeout,” which indicated that the nuts had been overtorqued during installation.
Probable Cause: A total loss of engine power due to maintenance personnel’s improper installation of the lower vacuum pump.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA14LA142 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/live/flight/N9417Z Location
Revision history:
Date/time | Contributor | Updates |
05-Mar-2014 23:39 |
Geno |
Added |
18-Mar-2014 16:23 |
Geno |
Updated [Phase, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 13:47 |
ASN Update Bot |
Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation