ASN Wikibase Occurrence # 165415
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Date: | Friday 11 April 2014 |
Time: | 10:07 |
Type: | Bowers Fly Baby 1A |
Owner/operator: | Private |
Registration: | N6054Q |
MSN: | 1068 |
Year of manufacture: | 2006 |
Total airframe hrs: | 32 hours |
Engine model: | Continental A65-8 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Mariposa-Yosemite Airport (KMPI), Mariposa, CA -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Mariposa, CA (MPI) |
Destination airport: | Mariposa, CA (MPI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The plans-built single-seat airplane had been constructed about 8 years before the accident by another individual, who had flown it about 30 hours before it was purchased by the current owner/pilot. In the year since the purchase, due to the low build-quality of the airplane, the pilot had made several modifications and repairs to the airplane. The accident flight was the pilot’s fifth flight in the airplane. Review of the pilot’s flight logbook indicated that his most recent flight review occurred about 7 years before the accident and that he had flown only 15 hours in the 2 years before the accident.
A witness reported that shortly after takeoff, when the airplane was about 3 miles from the airport, the engine began making a sound as if power was intermittently being interrupted. The nose of the airplane began to pitch up aggressively as it flew out of view. The wreckage location, wreckage distribution, and impact signatures indicated that the airplane struck the ground in a steep nose-low attitude, consistent with an aerodynamic stall event.
Postaccident examination of the carburetor revealed multiple maintenance-related discrepancies, any one of which could have resulted in the loss of engine power. Additionally, before the accident, the pilot reported to a friend that the airspeed indicator was not reliable and that the airplane exhibited roll control anomalies. Both of these conditions would have hindered the pilot’s ability to safely operate the airplane.
Probable Cause: The partial loss of engine power due to an improperly maintained carburetor and the pilot's subsequent failure to maintain aircraft control.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR14FA165 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=6054Q
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
11-Apr-2014 22:53 |
Geno |
Added |
12-Apr-2014 00:07 |
Geno |
Updated [Aircraft type, Source, Narrative] |
14-Apr-2014 23:02 |
Geno |
Updated [Registration, Cn, Operator, Source, Damage, Narrative] |
29-Apr-2014 05:57 |
Geno |
Updated [Time, Phase, Nature, Departure airport, Destination airport, Source] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 14:02 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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