ASN Wikibase Occurrence # 169097
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Date: | Saturday 23 August 2014 |
Time: | 12:10 |
Type: | Piper PA-28-180 Cherokee C |
Owner/operator: | Old Cherokee Llc |
Registration: | N9095J |
MSN: | 28-3133 |
Year of manufacture: | 1966 |
Total airframe hrs: | 2973 hours |
Engine model: | Lycoming O-360-A3A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Montgomery County Airpark, MD -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Gaithersburg, MD (GAI) |
Destination airport: | Caldwell, NJ (CDW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, before departing with full fuel tanks, he performed an engine run-up with no discrepancies noted. After taxiing the airplane onto the runway, the pilot applied partial power and then released the brakes. He then added full power, and the engine developed full power, the airplane accelerated normally, and all of the instruments were indicating normal. The pilot reported that the takeoff roll seemed normal. The airplane lifted off, and, when it reached about 100 ft above ground level, the engine surged once, which the pilot stated sounded similar to when the fuel-to-air ratio was leaned before shutdown. The pilot subsequently leveled off the airplane, and the engine operated normally and did not surge again. He continued the flight aware that there was insufficient runway remaining to land and allowed the airplane to accelerate and then climb. After the airplane ascended another 100 ft, the engine quit suddenly. At that point, due to trees, houses, and a road ahead, he decided to try to return to the airport. He attempted to troubleshoot the engine problem, including switching fuel tanks, but his actions did not restore engine power. He turned left toward an area north of the runway, and, at some point, he turned off the fuel selector and then bled off airspeed. The airplane impacted the ground with the left wing first followed by the left main landing gear. The pilot stated that he believed he was in controlled flight at the time of impact and that he had not stalled the airplane; this statement was corroborated by the stall warning light bulb filament not being stretched.
Impact damage to the crankshaft precluded an engine test run; however, examination of the engine and engine systems revealed no evidence of preimpact mechanical failure or malfunction. Examination of the fuel supply and fuel vent systems revealed no evidence of blockage, and the fuel selector tested satisfactorily. Data from the engine monitoring device showed a sharp decrease in fuel flow, followed by a slight increase, then another sudden decrease; however, the reason for the erratic fuel flow rate, which likely led to fuel starvation, could not be determined.
Although the environmental conditions at the time of the accident were favorable for serious carburetor icing at glide power or reduced power settings, the pilot reported that the engine developed full power during the takeoff; therefore, it is unlikely that carburetor icing resulted in the interruption of the fuel flow.
Probable Cause: The loss of engine power due to fuel starvation for reasons that could not be determined during postaccident examination of the fuel supply and fuel vent systems.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA14LA404 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Images:
Montgomery County Airpark, Gaithersburg MD
~ 2:30 p.m. 23 August 2014. Photo has been brightened.
Media:
Revision history:
Date/time | Contributor | Updates |
23-Aug-2014 17:29 |
gerard57 |
Added |
23-Aug-2014 18:42 |
harro |
Updated [Aircraft type, Registration, Cn, Location, Embed code] |
23-Aug-2014 18:42 |
harro |
Updated [Embed code, Damage] |
23-Aug-2014 20:40 |
Doug |
Updated [Time, Narrative, Photo, ] |
24-Aug-2014 06:26 |
RobertMB |
Updated [Aircraft type] |
24-Aug-2014 23:27 |
Aerossurance |
Updated [Source] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 18:59 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Embed code, Narrative] |
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