ASN Wikibase Occurrence # 171961
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Date: | Friday 5 December 2014 |
Time: | 11:10 |
Type: | Cessna 150J |
Owner/operator: | Eagle East Aviation Inc. |
Registration: | N50709 |
MSN: | 15069499 |
Year of manufacture: | 1968 |
Total airframe hrs: | 6506 hours |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | SE of Brookline Airport (NH16), Brookline, New Hampshire -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Lawrence, MA (LWM) |
Destination airport: | Keene, NH (EEN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The student pilot reported that the preflight inspection and engine run-up revealed no anomalies and that he subsequently departed for a solo cross-country flight. About 30 minutes into the flight, the student pilot observed low cloud ceilings and decided to return to his departure airport. Two minutes after turning the airplane back toward the airport, the engine power dropped below 2,000 rpm. The student pilot applied carburetor heat, but the engine power did not increase, so he proceeded to a nearby airport to initiate an emergency landing. However, the engine continued to lose rpm during the approach, so he decided to land in a small field. During the landing, the airplane impacted a wire and then the ground, which resulted in substantial damage to the right wing and fuselage.
Although the left magneto exhibited severe wear on the cam and burnt points, a single magneto failure would not have caused the loss of engine power. No other anomalies with the engine were found that would have precluded normal operation. Although atmospheric conditions at the time of the accident were favorable for the accumulation of carburetor icing at glide and cruise power, it could not be determined if carburetor ice was present when the loss of partial power occurred.
Probable Cause: The student pilot’s failure to maintain clearance from a wire during an off-airport landing following a partial loss of engine power for reasons that could not be determined during postaccident examination.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA15LA072 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/resources/registration/N50709 Location
Revision history:
Date/time | Contributor | Updates |
05-Dec-2014 18:43 |
Geno |
Added |
05-Dec-2014 23:50 |
Geno |
Updated [Source, Narrative] |
30-Dec-2014 02:22 |
Geno |
Updated [Time, Source, Damage, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 19:43 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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