Accident Cessna P210N N4873K,
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ASN Wikibase Occurrence # 174236
 
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Date:Sunday 18 January 2004
Time:05:52
Type:Silhouette image of generic P210 model; specific model in this crash may look slightly different    
Cessna P210N
Owner/operator:Private
Registration: N4873K
MSN: P21000352
Year of manufacture:1979
Total airframe hrs:3234 hours
Engine model:Continental TSIO-520-P7B
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Tucson, AZ -   United States of America
Phase: Landing
Nature:Private
Departure airport:Tucson, AZ (TUS)
Destination airport:Dallas, TX (DAL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During the landing roll, the airplane's left main landing gear collapsed and the airplane collided with a taxiway sign. While en route to his destination, the battery warning light illuminated, indicating that the electrical system was not charging. The pilot performed the emergency checklist items; however, the alternator would not reset. The pilot then reversed course to return to the departure airport. The pilot turned off all nonessential electrical equipment in an attempt to conserve battery power. The pilot extended the landing gear and 10 degrees of flaps, then turned the master switch off. The pilot later told responding airport police officers that he did not wait for the gear enunciator lights to turn green indicating that the landing gear was down-and-locked before shutting off the electrical master switch. As the airplane approached the airport, the pilot turned the master switch back on, but the battery had fully drained. The pilot said that he was unsure if the gear were down and locked so on final approach he pumped the emergency gear extension handle. During the landing roll, the left main gear collapsed. Post accident examination of the electrical system revealed that the main alternator field wire and power wire terminals were broken due to a vibration of the alternator. The alternator was not secure on its mounting bracket due to fretting on the forward portion of the alternator bracket housing, which had enlarged the holes into an oval shape. When the alternator and bracket were touched, the entire assembly would move.
Probable Cause: the failure of the electrical charging system and pilot's failure to verify that the gear was down-and-locked prior to the complete electrical system failure.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX04LA108
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20040203X00153&key=1

Location

Revision history:

Date/timeContributorUpdates
03-Mar-2015 17:45 Noro Added
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Dec-2017 17:34 ASN Update Bot Updated [Cn, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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