ASN Wikibase Occurrence # 176242
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 15 May 2015 |
Time: | 08:40 |
Type: | Cessna T206H Turbo Stationair |
Owner/operator: | Mid Continent Aircraft Corp |
Registration: | N164CS |
MSN: | T20609132 |
Year of manufacture: | 2014 |
Total airframe hrs: | 113 hours |
Engine model: | Lycoming TIO-540-AJ1A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Piggott Municipal Airport (7M7), Piggott, AR -
United States of America
|
Phase: | Take off |
Nature: | Executive |
Departure airport: | Piggott, AR (7M7) |
Destination airport: | Walnut Ridge, AR (KARG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:**This report was modified on August 28, 2016. Please see the docket for this accident to view the original report.**
The airline transport rated pilot reported that, after an en route stop, he planned to continue his cross-country personal flight. The pilot reported that, during takeoff and as the airplane was between about 20 and 30 ft above the ground, he felt the engine surge, and it then lost power. The airplane was traveling too fast to stop on the remaining runway, and it impacted a ditch at the end of the runway.
Examinations of the airframe and engine revealed that the left magneto was malfunctioning. During subsequent examination of the magneto, a section of a drill bit, which approximated the diameter of a timing pin, was found inside of it. A review of maintenance records revealed that the left magneto had been replaced 15.6 hours before the accident.
A review of engine monitor data revealed that the exhaust gas temperature spiked three times; two of the spikes were attributed to the "before takeoff" magneto checks. The third spike occurred during the takeoff and just before a power reduction. The data are consistent with the left magneto failing during the takeoff. The accident is consistent with maintenance personnel improperly using a drill bit as a timing pin to time the magneto before installing it on the engine. Maintenance personnel likely rotated the engine while the drill bit was still in the magneto, which resulted in a section of the drill bit then breaking off and eventually causing the magneto to fail.
Probable Cause: The loss of engine power due to a malfunctioning magneto. Contributing to the accident was maintenance personnel's improper use of a drill bit instead of a timing pin during magneto installation, which resulted in a section of the drill bit breaking off and ultimately to the magneto failure.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15LA233 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
20-May-2015 16:06 |
Geno |
Added |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 13:07 |
ASN Update Bot |
Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation