ASN Wikibase Occurrence # 176517
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Date: | Thursday 22 April 2004 |
Time: | 07:45 |
Type: | Piper PA-18-150 |
Owner/operator: | Private |
Registration: | N82943 |
MSN: | 18-7809028 |
Year of manufacture: | 1978 |
Total airframe hrs: | 1229 hours |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Minneapolis, MN -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Minneapolis, MN (MIC) |
Destination airport: | Maple Lake, MN (MGG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane impacted a power pole and trees during a forced landing after a loss of engine power during initial climb. According to the pilot, prior to the accident flight the airplane was completely fueled and fuel samples he took during the aircraft preflight were not contaminated with water. The pilot stated the airplane was taxied on the right main fuel tank, and he switched to the left fuel tank prior to takeoff as required by the pilot operating handbook. The pilot reported that he experienced an uneventful takeoff ground run, rotation, and initial climb until approximately 150 feet above ground level (agl) when the engine lost power suddenly. The pilot reported he switched fuel tank positions, verified the magneto switch was on both, and the throttle and mixture controls were fully advanced. The pilot reported, "Because of the suddenness and completeness of the loss of [engine] power, I suspected either fuel starvation or an ignition problem." The pilot stated, "I changed the tank selector at least two more times, and got ready to crash." The pilot stated that a landing on the departure runway was not an option and he maneuvered the airplane in between two houses prior to striking a power pole and several trees. A first responder reported the fuel selector was found in the "off" position upon his arrival at the accident site. The pilot reportedly said he did not reposition the fuel selector after the accident. The engine was subjected to an operational test-run. The engine started without hesitation and ran at idle power (~700 rpm) without any anomalies. The engine responded to brief throttle increases (~1,200 rpm) prior to being shutdown. The engine was not run above 1,200 rpm due to a damaged propeller.
Probable Cause: The pilot not verifying the position of the fuel selector prior to the takeoff, resulting in the loss of engine power during initial climb due to fuel starvation. Factors to the accident were the power pole and the trees.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI04CA108 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20040426X00512&key=1
History of this aircraft
Other occurrences involving this aircraft
30 March 2018 |
N101EB |
Private |
0 |
Butte Valley Airport (A32), Dorris, CA |
|
sub |
Runway excursion |
Location
Revision history:
Date/time | Contributor | Updates |
30-May-2015 17:16 |
Noro |
Added |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Dec-2017 17:53 |
ASN Update Bot |
Updated [Cn, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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