Loss of control Accident Beechcraft A36 Bonanza N985K,
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ASN Wikibase Occurrence # 176589
 
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Date:Tuesday 2 June 2015
Time:08:00
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36 Bonanza
Owner/operator:Bhb Of The Sandhills Llc
Registration: N985K
MSN: E-1947
Year of manufacture:1981
Total airframe hrs:3501 hours
Engine model:Continental IO-520-BB
Fatalities:Fatalities: 1 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Siler City Municipal Airport (KSCR), NC -   United States of America
Phase: Approach
Nature:Private
Departure airport:Pinehurst/southern Pines, NC (SOP)
Destination airport:Siler City, NC (SCR)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The purpose of the accident flight was to reposition the accident airplane in order to have maintenance performed on its alternator. The accident pilot planned to fly with the airplane's landing gear extended for the duration of the flight and used a handheld radio for communications, presumably because of the intermittent or non-functional state of the alternator. Another pilot, who was flying in his own airplane, accompanied the accident flight, and they arrived in the vicinity of the destination airport about the same time. As the accident pilot maneuvered his airplane to land, the accompanying pilot watched as the accident airplane flew a downwind traffic pattern leg very close to the runway, then entered a "tight" base-to-final turn. The airplane subsequently entered what the accompanying pilot described as an accelerated aerodynamic stall and descended in a nose-down attitude toward the ground. The airplane impacted trees and terrain about 500 ft short of the runway threshold. A postaccident examination of the wreckage revealed no evidence of any preimpact mechanical malfunctions or failures, with the exception of the alternator, which failed a diagnostic test run.

Probable Cause: The pilot's failure to maintain adequate airspeed and his exceedance of the airplane's critical angle of attack while maneuvering for landing, which resulted in an aerodynamic stall.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA15LA231
Status: Investigation completed
Duration: 2 years and 11 months
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=985K

Location

Images:


Photo: NTSB

Revision history:

Date/timeContributorUpdates
02-Jun-2015 14:42 Geno Added
02-Jun-2015 16:27 Geno Updated [Registration, Cn, Operator, Departure airport, Source, Damage, Narrative]
02-Jun-2015 18:28 Geno Updated [Registration, Cn, Operator, Source]
02-Jun-2015 18:30 Geno Updated [Source, Embed code]
03-Jun-2015 14:00 Anon. Updated [Total fatalities]
03-Jun-2015 14:01 harro Updated [Location, Narrative]
03-Jun-2015 14:02 harro Updated [Embed code]
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
16-May-2018 15:38 ASN Update Bot Updated [Operator, Nature, Departure airport, Destination airport, Source, Embed code, Narrative]
16-May-2018 17:54 harro Updated [Source, Embed code, Narrative, Photo, ]

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