ASN Wikibase Occurrence # 176589
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Date: | Tuesday 2 June 2015 |
Time: | 08:00 |
Type: | Beechcraft A36 Bonanza |
Owner/operator: | Bhb Of The Sandhills Llc |
Registration: | N985K |
MSN: | E-1947 |
Year of manufacture: | 1981 |
Total airframe hrs: | 3501 hours |
Engine model: | Continental IO-520-BB |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Siler City Municipal Airport (KSCR), NC -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Pinehurst/southern Pines, NC (SOP) |
Destination airport: | Siler City, NC (SCR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The purpose of the accident flight was to reposition the accident airplane in order to have maintenance performed on its alternator. The accident pilot planned to fly with the airplane's landing gear extended for the duration of the flight and used a handheld radio for communications, presumably because of the intermittent or non-functional state of the alternator. Another pilot, who was flying in his own airplane, accompanied the accident flight, and they arrived in the vicinity of the destination airport about the same time. As the accident pilot maneuvered his airplane to land, the accompanying pilot watched as the accident airplane flew a downwind traffic pattern leg very close to the runway, then entered a "tight" base-to-final turn. The airplane subsequently entered what the accompanying pilot described as an accelerated aerodynamic stall and descended in a nose-down attitude toward the ground. The airplane impacted trees and terrain about 500 ft short of the runway threshold. A postaccident examination of the wreckage revealed no evidence of any preimpact mechanical malfunctions or failures, with the exception of the alternator, which failed a diagnostic test run.
Probable Cause: The pilot's failure to maintain adequate airspeed and his exceedance of the airplane's critical angle of attack while maneuvering for landing, which resulted in an aerodynamic stall.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA15LA231 |
Status: | Investigation completed |
Duration: | 2 years and 11 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=985K Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
02-Jun-2015 14:42 |
Geno |
Added |
02-Jun-2015 16:27 |
Geno |
Updated [Registration, Cn, Operator, Departure airport, Source, Damage, Narrative] |
02-Jun-2015 18:28 |
Geno |
Updated [Registration, Cn, Operator, Source] |
02-Jun-2015 18:30 |
Geno |
Updated [Source, Embed code] |
03-Jun-2015 14:00 |
Anon. |
Updated [Total fatalities] |
03-Jun-2015 14:01 |
harro |
Updated [Location, Narrative] |
03-Jun-2015 14:02 |
harro |
Updated [Embed code] |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
16-May-2018 15:38 |
ASN Update Bot |
Updated [Operator, Nature, Departure airport, Destination airport, Source, Embed code, Narrative] |
16-May-2018 17:54 |
harro |
Updated [Source, Embed code, Narrative, Photo, ] |
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