ASN Wikibase Occurrence # 177365
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Date: | Saturday 27 June 2015 |
Time: | 08:00 |
Type: | Cessna TR182 Turbo Skylane RG |
Owner/operator: | Private |
Registration: | N4751S |
MSN: | R18201413 |
Year of manufacture: | 1979 |
Total airframe hrs: | 2170 hours |
Engine model: | Lycoming O-540-L3C5D |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Casper/Natrona County Int'l Airport (KCPR), Casper, WY -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Casper, WY (KCPR) |
Destination airport: | Jackson, WY (KJAC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot was conducting a cross-country personal flight. Immediately after takeoff, the engine lost power. The pilot and pilot-rated passenger attempted to restore engine power but were unsuccessful. The airplane was unable to return to the airport, and the pilot conducted a forced landing, during which the airplane impacted terrain beyond the airport perimeter fence.
An examination of the engine revealed that the sheath for the carburetor heat cable was separated from the clamp. A black rubber adhesive was found at the joint between the sheath and the clamp, but it was not securing the clamp to the joint. The carburetor heat at the carburetor was partially on, and the position could not be changed when actuated by the control knob in the cabin. An examination of the airframe, engine, and related systems revealed no further anomalies.
The weather conditions at the time of the accident were conducive to the accumulation of serious carburetor icing at glide power; however, it could not be determined whether carburetor icing played a role in the loss of engine power. Even if carburetor icing had not accumulated, the separation of the sheath from the clamp would have prevented the proper operation of the carburetor heat, and the partial carburetor heat would have resulted in the loss of engine power at takeoff.
Probable Cause: The improper repair of the carburetor heat cable sheath to clamp joint, which prevented the proper operation of the carburetor heat and resulted in the loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15LA284 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N4751S Location
Revision history:
Date/time | Contributor | Updates |
27-Jun-2015 23:53 |
Geno |
Added |
28-Jun-2015 00:03 |
Geno |
Updated [Source, Damage, Narrative] |
29-Jun-2015 18:02 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Source] |
02-Jul-2015 18:38 |
Geno |
Updated [Nature, Destination airport, Source, Narrative] |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 13:42 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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