ASN Wikibase Occurrence # 178098
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Date: | Monday 27 July 2015 |
Time: | 19:47 |
Type: | Wheeler Express |
Owner/operator: | Private |
Registration: | N3FC |
MSN: | 1001 |
Year of manufacture: | 2008 |
Total airframe hrs: | 481 hours |
Engine model: | Lycoming IO-540-C4B5 |
Fatalities: | Fatalities: 3 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Grange Township in Pipestone County near Holland, MN -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Pipestone, MN (PQN) |
Destination airport: | Pipestone, MN (PQN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot departed with two passengers for a personal, local flight in a Wheeler Express amateur-built airplane. Air traffic control data indicate that, after departing the airport, the airplane climbed and performed several maneuvers. A review of onboard flight data revealed that the airplane then maneuvered into a nose-high attitude while in a steep, right turn. As the airspeed decelerated below stall speed and the turn steepened, the airplane pitched nose down and entered a prolonged, right-turning spin until ground impact. Examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation.
Previous flight testing of a Wheeler Express kit airplane similar to the accident airplane revealed that it had poor yaw stability at low airspeed due to the aerodynamic design of the tail section. The testing also revealed that, during poststall and high-yaw maneuvering, the horizontal tail and elevators appeared to have an inadequate effect. Following bankruptcy of the original kit manufacturer, a variant of the Wheeler Express kit airplane was developed using the same wing and fuselage as the accident model but with a larger tail that had 40 percent more wetted area to provide additional yaw stability at low airspeed.
Probable Cause: The pilot’s failure to maintain adequate airspeed during a high-pitch, steep right turn, which resulted in the exceedance of the airplane’s critical angle-of-attack and a subsequent aerodynamic stall, loss of control, and impact with terrain. Contributing to the accident was the airplane’s design, which resulted in poor yaw stability at low airspeed.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15FA321 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=3FC Location
Revision history:
Date/time | Contributor | Updates |
28-Jul-2015 15:23 |
Geno |
Added |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 15:02 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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