ASN Wikibase Occurrence # 180980
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Date: | Monday 2 November 2015 |
Time: | 14:24 |
Type: | Bell 206B JetRanger II |
Owner/operator: | Applebee Aviation Inc |
Registration: | N22743 |
MSN: | 3624 |
Year of manufacture: | 1982 |
Total airframe hrs: | 18443 hours |
Engine model: | Rolls Royce 250-C20B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sheridan, Polk County, OR -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | External load operation |
Departure airport: | Dallas, OR |
Destination airport: | Dallas, OR |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot of the helicopter reported that, after he released the external load of trees in the loading zone and about 50 ft above ground level, it seemed like the engine experienced a partial loss of power. The pilot stated that he heard an abnormal noise as the helicopter began to spin to the right, and the low rotor rpm warning light illuminated. The pilot jettisoned the external load line and rolled the throttle toward a closed position in order to counteract the yawing motion, with no response noted. The pilot then initiated an autorotation; during the landing sequence, the helicopter impacted a tree and came to rest upright in a nose-high position. The pilot further stated that, after the helicopter came to rest, he noted that the engine was at a “very slow idle” and he had to shut down the engine. Postaccident examination of the helicopter revealed no evidence of any preexisting mechanical anomalies that would have precluded normal operation. The engine was removed and installed in an engine test cell and ran throughout various power settings.
The airframe fuel filter was removed. The filter element was almost black. The fuel removed was dark, and debris was observed within the fuel filter bowl. The fuel sample from the filter housing was tested and found to be within Jet A specifications. The debris noted within the sample contained various metals, the source of which could not be determined. Given that fuel was found throughout the fuel system, it is unlikely that the debris in the filter resulted in a blockage and restriction of fuel flow; however, the reason for the partial loss of engine power could not be determined.
Probable Cause: A loss of engine power for reasons that could not be determined based on the available information.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR16LA020 |
Status: | Investigation completed |
Duration: | 2 years and 3 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
03-Nov-2015 17:41 |
gerard57 |
Added |
03-Nov-2015 17:42 |
harro |
Updated [Aircraft type, Registration, Cn, Location, Source, Damage] |
21-Dec-2015 13:05 |
Aerossurance |
Updated [Source, Narrative] |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Feb-2018 13:51 |
ASN Update Bot |
Updated [Operator, Nature, Departure airport, Destination airport, Source, Narrative] |
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