ASN Wikibase Occurrence # 181562
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Date: | Thursday 26 July 2012 |
Time: | 14:45 |
Type: | McDonnell Douglas MD 500E (369E) |
Owner/operator: | Wilson Construction Co |
Registration: | N427WC |
MSN: | 0188E |
Year of manufacture: | 1986 |
Total airframe hrs: | 2757 hours |
Engine model: | Rolls-Royce 250-C20 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | 8 miles east of The Dalles, Oregon -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | External load operation |
Departure airport: | The Dalles, OR (KDLS) |
Destination airport: | The Dalles, OR (KDLS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The operator reported that the helicopter was in an 80-ft hover and had begun lifting and dragging the ends of winch lines used to pull power cables across sloping terrain when the engine lost power. The pilot jettisoned the external load as the helicopter began to descend rapidly. The helicopter’s tail boom contacted the ground first and was then cut by the main rotor system, the skids separated from the fuselage, and the helicopter then came to rest on its right side. Several witnesses reported that the engine was still running on the ground after the impact.
Postaccident examination and operational testing of the engine revealed no anomalies that would have precluded normal operation. During previous investigations of similar accidents, it was determined that the fuel tank supply pickup can become unported with a fuel load of less than 151 lbs when pitch-and-roll attitudes approach 20 degrees; the operator reported that about 117 lbs of fuel was recovered from the helicopter. It is likely that the fuel tank supply pickup unported while the helicopter was maneuvering, which led to fuel starvation and the subsequent loss of engine power.
Probable Cause: The loss of engine power due to fuel starvation, which resulted from the fuel tank supply pickup becoming unported while the helicopter was pulling power lines.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR12LA328 |
Status: | Investigation completed |
Duration: | 3 years and 3 months |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/resources/registration/N427WC Location
Revision history:
Date/time | Contributor | Updates |
21-Nov-2015 17:10 |
Aerossurance |
Added |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:57 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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