Accident Cessna U206F N14C,
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ASN Wikibase Occurrence # 182059
 
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Date:Thursday 1 May 1997
Time:12:01 LT
Type:Silhouette image of generic C206 model; specific model in this crash may look slightly different    
Cessna U206F
Owner/operator:Jay Hawk Air
Registration: N14C
MSN: U20602803
Total airframe hrs:9475 hours
Engine model:Continental IO-520-F
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location: 17 miles SW of Hope, Alaska -   United States of America
Phase: Unknown
Nature:Unknown
Departure airport:Montague Island, AK
Destination airport:Anchorage, AK (MRI)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported he was starting a descent to his destination airport when the engine began to lose power. He said he was unable to restart the engine, and made a forced landing into trees. The pilot related he had been flying the airplane with the left fuel tank selected, and he didn't recall if he switched to the right tank during the emergency descent. A passenger seated in the right front seat stated the left fuel gauge was indicating empty, and that the right tank fuel gauge was indicating full. He said the fuel selector was on the left tank, and when he told the pilot he should switch fuel tanks, the pilot reportedly told him to 'relax.' The passenger stated that the pilot did not switch tanks. Postaccident inspection disclosed the left fuel tank contained an unusable quantity of fuel, and the right tank was full. The airplane's engine was removed from the airplane, as well as the electric fuel boost pump. The engine was started and ran on a test stand without any observed mechanical anomalies. The fuel pump was also tested and found functional.

Probable Cause: a loss of engine power resulting from fuel starvation due to the pilot's improper positioning of the fuel selector, and the pilot's failure to identify and correct the deficiency during the ensuing emergency descent.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC97LA065
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB ANC97LA065

History of this aircraft

Other occurrences involving this aircraft
9 August 1994 N14C Ace Flyers Inc. 0 Skwentna, AK sub

Location

Revision history:

Date/timeContributorUpdates
07-Dec-2015 07:21 JINX Added
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
08-Apr-2024 15:39 ASN Update Bot Updated [Time, Cn, Other fatalities, Phase, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

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