ASN Wikibase Occurrence # 182059
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Date: | Thursday 1 May 1997 |
Time: | 12:01 LT |
Type: | Cessna U206F |
Owner/operator: | Jay Hawk Air |
Registration: | N14C |
MSN: | U20602803 |
Total airframe hrs: | 9475 hours |
Engine model: | Continental IO-520-F |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | 17 miles SW of Hope, Alaska -
United States of America
|
Phase: | Unknown |
Nature: | Unknown |
Departure airport: | Montague Island, AK |
Destination airport: | Anchorage, AK (MRI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported he was starting a descent to his destination airport when the engine began to lose power. He said he was unable to restart the engine, and made a forced landing into trees. The pilot related he had been flying the airplane with the left fuel tank selected, and he didn't recall if he switched to the right tank during the emergency descent. A passenger seated in the right front seat stated the left fuel gauge was indicating empty, and that the right tank fuel gauge was indicating full. He said the fuel selector was on the left tank, and when he told the pilot he should switch fuel tanks, the pilot reportedly told him to 'relax.' The passenger stated that the pilot did not switch tanks. Postaccident inspection disclosed the left fuel tank contained an unusable quantity of fuel, and the right tank was full. The airplane's engine was removed from the airplane, as well as the electric fuel boost pump. The engine was started and ran on a test stand without any observed mechanical anomalies. The fuel pump was also tested and found functional.
Probable Cause: a loss of engine power resulting from fuel starvation due to the pilot's improper positioning of the fuel selector, and the pilot's failure to identify and correct the deficiency during the ensuing emergency descent.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC97LA065 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB ANC97LA065
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
07-Dec-2015 07:21 |
JINX |
Added |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 15:39 |
ASN Update Bot |
Updated [Time, Cn, Other fatalities, Phase, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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