Accident Aeronca 7BCM (L-16A) N7620B,
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ASN Wikibase Occurrence # 186883
 
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Date:Saturday 30 April 2016
Time:10:57
Type:Silhouette image of generic CH7A model; specific model in this crash may look slightly different    
Aeronca 7BCM (L-16A)
Owner/operator:Commemorative Air Force
Registration: N7620B
MSN: 7BCM-384
Year of manufacture:1947
Total airframe hrs:1600 hours
Engine model:Continental C85-8F
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Fayette County, east of Tyrone, GA -   United States of America
Phase: Landing
Nature:Executive
Departure airport:Peachtree City, GA (FFC)
Destination airport:Peachtree City, GA (FFC)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airline transport pilot was conducting a revenue sightseeing flight with one passenger onboard. During cruise flight, while the airplane was level at 3,000 ft mean sea level, the engine began to lose power. The pilot applied carburetor heat with no improvement; the engine speed remained at 2,000 rpm. He then turned the carburetor heat off and checked the magnetos and noted no significant change in performance. He then reapplied carburetor heat with no improvement; the pilot left the heat on for the remainder of the flight. The airplane would not maintain altitude, so he conducted a forced landing in a grass field. After touchdown, the airplane nosed down in high vegetation, and the main landing gear collapsed. The airplane sustained structural damage to the forward fuselage and engine firewall.
Postaccident examination of the airframe and engine revealed no evidence of preimpact mechanical failures or malfunctions that would have precluded normal operation, and there was sufficient fuel onboard at the time of the accident. Although the weather conditions at the time of the accident were conducive to serious carburetor icing at glide power, the pilot applied carburetor heat twice, which should have melted any existing ice, but power was not restored. Therefore, the investigation could not determine the reason for the partial loss of engine power.

Probable Cause: A partial loss of engine power during cruise flight for reasons that could not be determined because postaccident examination of the engine revealed no anomalies that would have precluded normal operation.


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA16LA172
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=7620B

Location

Revision history:

Date/timeContributorUpdates
01-May-2016 01:23 Geno Added
01-May-2016 01:24 Geno Updated [Narrative]
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
19-Aug-2017 15:08 ASN Update Bot Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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