ASN Wikibase Occurrence # 195274
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Date: | Tuesday 17 March 2015 |
Time: | 14:40 UTC |
Type: | de Havilland Canada DHC-8-402Q Dash 8 |
Owner/operator: | SpiceJet |
Registration: | VT-SUI |
MSN: | 4395 |
Fatalities: | Fatalities: 0 / Occupants: 71 |
Aircraft damage: | None |
Category: | Incident |
Location: | Hyderabad-Rajiv Gandhi International Airport (HYD/VOHS) -
India
|
Phase: | Taxi |
Nature: | Passenger - Scheduled |
Departure airport: | Madurai Airport (IXM/VOMD) |
Destination airport: | Hyderabad-Rajiv Gandhi International Airport (HYD/VOHS) |
Investigating agency: | DGCA India |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A SpiceJet DHC-8-402Q aircraft, VT-SUI, was engaged in a scheduled return flight from Hyderabad to Colombo via Madurai, India (SG3313/3314).
The first three sectors were uneventful. However during the fourth sector, from Madurai to Hyderabad, after landing on runway 09R a fuel smell was noticed by the cockpit and cabin crew.
After the aircraft had reached the parking bay, ground staff started running and gave hand signals to the cockpit crew to evacuate and showed some urgency in their behaviour. As a precautionary action the pilot in command called for evacuation. There was an AME on board the aircraft seated in 1B who operated the right hand emergency exit (R1 Door) without any command from flight or cabin crew. None of the passenger was injured during the evacuation.
After evacuation the pilot in command observed smoke coming out of no. 2 engine. Some fuel had also spilled out of the engine. However there was no fire. The pilot reported that all engine parameters were normal except that he observed a low fuel level on engine no.2 by approx 200 kgs.
The marshaller at the parking bay reported that he did not observe smoke when he was marshalling the aircraft. After the aircraft stopped and the engineering staff was putting the chocks, he observed heavy smoke from engine no. 2.
After the incident the fuel oil heat exchanger was inspected. All internal components showed excess wear. The oil circuit was found to be contaminated with fuel. The fuel circuit also showed some contamination.
Probable cause of the Incident:
The cause for the fuel vapours in the aircraft cabin and dense white smoke from #2 engine was attributed to the faulty fuel heater.
Accident investigation:
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| |
Investigating agency: | DGCA India |
Report number: | |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
http://dgca.nic.in/accident/reports/incident/VT-SUI.pdf Revision history:
Date/time | Contributor | Updates |
08-May-2017 18:09 |
harro |
Added |
08-May-2017 18:13 |
harro |
Updated [Narrative] |
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