ASN Wikibase Occurrence # 195916
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Date: | Sunday 4 June 2017 |
Time: | 09:17 |
Type: | Titan T-51 Mustang |
Owner/operator: | Private |
Registration: | N51FB |
MSN: | MO4XXXS0HK0052 |
Year of manufacture: | 2015 |
Total airframe hrs: | 43 hours |
Engine model: | Suzuki H27A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Phoenix Goodyear Airport (KGYR), Goodyear, AZ -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Phoenix Goodyear Airport, AZ (GYR/KGYR) |
Destination airport: | Phoenix Goodyear Airport, AZ (GYR/KGYR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airline transport pilot indicated that, immediately after takeoff for the local flight, the experimental, amateur-built airplane began to vibrate. As he transitioned the airplane to the downwind leg, the vibration increased, and the engine then experienced an overspeed and lost all power. The cockpit filled with smoke and the pilot subsequently performed a forced off-airport landing, which resulted in substantial damage to the left wing and aft fuselage.
The airplane had accrued about 43 flight hours since its construction, which was completed about 2 years before the accident.
Examination of the propeller speed reduction gearbox revealed that the teeth of the input drive gear had separated, which caused a loss of drive continuity to the propeller. The drive and idler gears did not appear to meet the manufacturer's case hardness requirements; however, evidence suggests that the gearbox had undergone severe heat buildup during the failure sequence, which may have subsequently altered the hardness. Oil starvation or exhaustion likely did not occur, as the gearbox bearings were intact and largely undamaged. Due to damage sustained to the gears, an accurate assessment of the initial failure mode could not be determined. Thus, the investigation could not determine the reason for the failure of the propeller speed reduction gearbox input drive gear.
Probable Cause: Failure of the propeller speed reduction gearbox input drive gear during the airplane’s initial climb for reasons that could not be determined due to extensive damage.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR17LA121 |
Status: | Investigation completed |
Duration: | 2 years and 5 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=51FB Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
04-Jun-2017 21:10 |
Geno |
Added |
04-Jun-2017 22:05 |
Iceman 29 |
Updated [Time, Source, Embed code] |
27-Nov-2019 07:15 |
ASN Update Bot |
Updated [Time, Operator, Nature, Departure airport, Destination airport, Source, Embed code, Damage, Narrative, Accident report, ] |
27-Nov-2019 07:37 |
harro |
Updated [Departure airport, Destination airport, Source, Embed code, Narrative, Photo] |
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