ASN Wikibase Occurrence # 198625
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Date: | Friday 16 September 2016 |
Time: | 16:30 |
Type: | Airtime Cygnet |
Owner/operator: | Private |
Registration: | N145AT |
MSN: | 0101 |
Year of manufacture: | 2015 |
Total airframe hrs: | 200 hours |
Engine model: | Rotax 912 ULS |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Venice, FL -
United States of America
|
Phase: | Take off |
Nature: | Training |
Departure airport: | Venice, FL (VNC) |
Destination airport: | Venice, FL (VNC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor in the amphibious float-equipped, weight-shift aircraft reported that the accident flight was the third flight with the student pilot, and the student pilot’s first flight in the front seat. He further reported that during the takeoff roll they “began to [lose] the center line to the left and then to the right.” He reported that in this particular aircraft, to turn to the right you push the left pedal and to turn to the left you push the right pedal. He instructed the student pilot to release the throttle. He then attempted to “take the controls back and keep the [aircraft] on the runway”, but was unsuccessful. The aircraft veered off the runway to the right, the right float impacted grass, and the aircraft spun 180 degrees.
The student pilot reported that he told the flight instructor that he would “follow along with him on the controls during the takeoff to feel how he was moving them”. He further reported that when the aircraft veered off the runway to the right, he “took [his] hands off the controls” to allow the flight instructor to correct for the veer.
The aircraft sustained substantial damage to the right lift strut.
The flight instructor reported no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable Cause: The student pilot’s failure to maintain directional control during the takeoff roll and the flight instructor’s delayed remedial action, which resulted in a runway excursion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA16CA498 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
19-Aug-2017 13:34 |
ASN Update Bot |
Added |
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