Accident McDonnell Douglas MD-11F N584FE,
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ASN Wikibase Occurrence # 198779
 
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Date:Tuesday 24 February 2015
Time:06:16
Type:Silhouette image of generic MD11 model; specific model in this crash may look slightly different    
McDonnell Douglas MD-11F
Owner/operator:FedEx
Registration: N584FE
MSN: 48436/483
Year of manufacture:1992
Engine model:GE CF6-80 SERIES
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: None
Category:Accident
Location:St. Louis, MO -   United States of America
Phase: En route
Nature:Cargo
Departure airport:Memphis, TN (MEM)
Destination airport:Minneapolis, MN (MSP)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During cruise flight, the crew received a fire warning from the cargo compartment indicating that the fire suppression system had activated, along with hearing loud sounds from the cargo compartment. The flight crew elected to divert to St. Louis. Although the activation of the fire suppression was a false alarm, the decision to divert was prudent and correct. During the approach the crew made the decision to evacuate the airplane after landing, briefed the passengers in the courier area, and reviewed the evacuation checklist in the Quick Reference Handbook (QRH). The diversion and subsequent landing were performed without issue. After exiting the runway, and bringing the airplane to a stop in a safe area, the crew initiated an emergency evacuation using the left forward door (1L). The door opened, however, the 1L escape slide/raft did not fully deploy, appearing to be hung up on a strap. The first officer attempted to free it and the fire/rescue crew pulled on the slide and it appeared to inflate. However, because the slide inflation sequence had been interrupted, it was significantly underinflated and unable to support the weight of the crewmember, resulting in a serious injury. Post-incident examination of the 1L slide/raft was unable to determine the causes for the slide/raft to not inflate to full extension.
Probable Cause: a partial inflation of the 1L escape slide/raft due to undetermined reasons resulting in insufficient capability to support the weight of the crewmember.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DCA15FA073
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB

History of this aircraft

Other occurrences involving this aircraft
2 April 1995 N1768D American Airlines 0 New York-John F. Kennedy International Airport, NY (JFK/KJFK) non
Engine failure
13 July 1996 N1768D American Airlines 0 Westerly, RI non
21 June 2023 N584FE FedEx Express 0 near Toronto-Pearson International Airport, ON (YYZ/CYYZ) unk
Reverse issue

Location

Revision history:

Date/timeContributorUpdates
19-Aug-2017 15:08 ASN Update Bot Added
25-Nov-2017 12:47 harro Updated [Other fatalities, Phase]

Corrections or additions? ... Edit this accident description

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