ASN Wikibase Occurrence # 199273
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Date: | Monday 28 August 2017 |
Time: | 11:10 |
Type: | Pacific Aerospace 750XL |
Owner/operator: | Private |
Registration: | N750UP |
MSN: | 133 |
Year of manufacture: | 2007 |
Total airframe hrs: | 4910 hours |
Engine model: | Pratt & Whitney PT6A-34 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Harvest, Alabama -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Perkasie-Pennridge Airport, PA (KCKZ) |
Destination airport: | Huntsville International Airport, AL (HSV/KHSV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot was conducting a cross-country flight to deliver the airplane to a maintenance facility. The airplane departed with full fuel tanks. The pilot stated that, as the airplane neared the planned fuel stop airport, he thought that there was adequate fuel remaining to reach the maintenance facility, so he did not stop to refuel and continued to the destination. About 4 hours 23 minutes into the flight, which was past the expected fuel exhaustion time of about 4 hours 18 minutes (assuming a fuel burn of 50 gallons per hour, which the pilot used for his initial flight planning), the pilot declared an emergency and advised an air traffic controller that the airplane was out of fuel. The controller provided information to the pilot about nearby airports, but the airplane would not have been able to reach any of them, so the pilot initiated a forced landing to a field. Before touchdown in the field, the pilot descended to avoid power lines ahead, but the airplane hit one of the lines. The airplane touched down in the field, impacted an embankment, and came to rest upright on a road. The airplane sustained substantial damage.
A small amount of fuel was observed on the ground at the accident site, and residual fuel was found in the two forward fuel tanks. Although the amount of the fuel could not be quantified, it was likely equivalent to the unusable fuel amount. Examination of the airframe fuel system components, including the fuel filter, the environmental collector tank, and the fuel lines in the engine compartment, revealed no fuel, which is consistent with fuel exhaustion. Therefore, it is likely that the pilot’s improper decision to not to refuel as planned and his improper in-flight fuel planning led to the loss of all engine power due to fuel exhaustion
Probable Cause: The pilot's improper decision to not stop and refuel the airplane as planned and his improper in-flight fuel planning, which resulted in a total loss of engine power due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA17LA302 |
Status: | Investigation completed |
Duration: | 2 years and 3 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Images:
Photo: FAA
Revision history:
Date/time | Contributor | Updates |
29-Aug-2017 15:18 |
gerard57 |
Added |
30-Aug-2017 11:44 |
RobertMB |
Updated [Cn] |
30-Aug-2017 12:40 |
Anon. |
Updated [Departure airport] |
31-Aug-2017 12:36 |
Anon. |
Updated [Total occupants, Location, Source, Narrative] |
22-Dec-2019 14:15 |
ASN Update Bot |
Updated [Time, Departure airport, Destination airport, Source, Narrative, Accident report, ] |
22-Dec-2019 19:59 |
harro |
Updated [Departure airport, Destination airport, Narrative, Photo] |
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