ASN Wikibase Occurrence # 200505
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Date: | Friday 4 December 1998 |
Time: | 16:55 LT |
Type: | Stinson 10A |
Owner/operator: | Lake Clark Air Inc. |
Registration: | N36755 |
MSN: | 8168 |
Year of manufacture: | 1941 |
Total airframe hrs: | 4359 hours |
Engine model: | Lycoming O-320-A2B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | 14 km E of Nondalton, AK -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | Port Alsworth, AK |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The certificated commercial pilot, and the sole passenger, departed for an on-demand air taxi flight over remote terrain. The passenger was conducting moose counting research for the Alaska Department of Fish and Game. The airplane carried four hours of fuel divided between two wing mounted fuel tanks. Each fuel tank is equipped with an electric fuel gauge. After flying for two hours with the left fuel tank selected, the fuel in the left tank was almost exhausted, and the pilot switched to the right fuel tank. He then flew for about 1.5 hours on the right tank before the engine suddenly quit. The pilot switched back to the left tank and climbed to about 1,000 feet above the ground. After about 6 minutes on the left tank, the engine quit running again. The pilot selected an emergency landing area on a small, frozen pond. The surface of the pond contained slushy ice and drifted snow. During the landing roll, the airplane entered deep snow and nosed over. The passenger reported she flew in the accident airplane two days before the accident. During that flight, she noticed the right fuel gauge in the airplane was inoperative. During the accident flight, two days later, she again noticed the right fuel gauge was still inoperative. Following recovery of the airplane, evidence of fuel staining was observed on the upper surface of the right wing, adjacent to the right fuel cap.
Probable Cause: The pilot's continued operation of the airplane with known deficiencies, a failure of company maintenance personnel to replace an inoperative fuel gauge, and subsequent fuel exhaustion. Factors in the accident were siphoning of fuel from the right wing fuel cap, and slush covered terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC99LA015 |
Status: | Investigation completed |
Duration: | 2 years and 2 months |
Download report: | Final report |
|
Sources:
NTSB ANC99LA015
Location
Revision history:
Date/time | Contributor | Updates |
21-Oct-2017 18:35 |
TB |
Added |
13-Sep-2023 11:01 |
Ron Averes |
Updated |
04-Apr-2024 12:42 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Departure airport, Source, Narrative, Category, Accident report] |
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