ASN Wikibase Occurrence # 202052
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Date: | Friday 26 March 1999 |
Time: | 13:10 LT |
Type: | Cessna T210L |
Owner/operator: | Wings Aloft |
Registration: | N93377 |
MSN: | 210-60381 |
Total airframe hrs: | 3130 hours |
Engine model: | Continental TSIO-520-H |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Port Angeles, WA -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | Seattle, WA (KBFI) |
Destination airport: | (KCLM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the annual inspection, leaking fuel tank caps and a water-contaminated fuel system were discovered. After completion of the annual, to include replacement of the caps and extensive actions to purge the system of any contamination, the pilot was asked to take the airplane on a post-maintenance test flight. During this flight, the pilot, who had been made aware that there had been significant water contamination of the fuel system, was supposed to make sure the aircraft ran properly and that there was nothing wrong with it. The pilot operated the engine prior to takeoff with the left fuel system selected, but did not select the right tank to see if he could detect any residual water contamination in that side of the system. He also did not test the right system while at altitude or when at a location where he could easily reach an airport if the engine lost power. After descending toward his en route destination, the pilot switched to the right fuel system and soon thereafter the engine experienced a complete loss of power. Unable to extend the glide to the airport, the pilot was able to land on a municipal baseball field. Although the touchdown was successful, the pilot was unable to get the airplane stopped prior to impacting the backstop.
Probable Cause: The pilot's improper in-flight decision which resulted in a loss of power due to a contaminated fuel system. Factors include unsuitable terrain and the fence.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA99LA044 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB SEA99LA044
Location
Revision history:
Date/time | Contributor | Updates |
26-Nov-2017 10:54 |
ASN Update Bot |
Added |
08-Apr-2024 08:08 |
ASN Update Bot |
Updated [Time, Cn, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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